CONTINUOUS IMPROVEMENT OF DRILLING ULTRA-SHALLOW HORIZONTAL WELL THROUGH LEAN SIX SIGMA METHODOLOGY

Petrus Tri Wahyudi, G. Yudoko
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引用次数: 1

Abstract

Low oil price environment impacted to business of Oil and Gas Company including PT. SDEC. However, PT. SDEC was able securing limited and fixed capital budget to drill well and had committed to drill certain well number to Government of Indonesia. When the initial 12 wells were completed with longer cycle time (average 9.9 days/well) than business plan (7.5 days/well) and also higher cost, the problem became more complex because company need to complete well as per commitment and in other hand no additional capital will be spent by parent company if actual expenditure exceeded the initial budget. Company assigned a team to solve the problem through Lean Six Sigma. Through strong collaboration among team, the project execution performance was improved (the Cp of drilling cycle time was improved from 0.06 to 1.08). As the result of this project save cost around $ 2.8 million.
精益六西格玛方法在超浅层水平井钻井中的持续改进
低油价环境对包括PT. SDEC在内的油气公司的业务产生了影响。然而,PT. SDEC能够获得有限和固定的钻井资本预算,并承诺向印度尼西亚政府钻探一定数量的井。当最初的12口井完成时,周期时间(平均9.9天/口)比商业计划(7.5天/口)长,成本也更高,问题变得更加复杂,因为公司需要按照承诺完成井,另一方面,如果实际支出超过了初始预算,母公司将不会花费额外的资金。公司指派了一个小组通过精益六西格玛解决问题。通过团队之间的紧密协作,提高了项目执行绩效(钻井周期时间Cp由0.06提高到1.08)。由于这个项目节省了大约280万美元的成本。
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