Layout Redesign to Eliminate Stagnation Using Blocplan to Increase Production Efficiency

OPSI Pub Date : 2022-12-30 DOI:10.31315/opsi.v15i2.8023
D. Wicaksono, I. Setiawan, Fitriana Lestari Hasan
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引用次数: 0

Abstract

The rapid growth of the automotive industry was also followed by growth in subsidiary companies. One of the subsidiary companies is a company that produces auto parts such as wheels. Sales volume in 2021 increased to more than 2 million products while for 2022 to April it was more than 1 million products. High demand is not accommodated due to inadequate production capacity, one of which is the machining area. This study aims to increase efficiency by redesigning the layout of the factory which is considered to increase production results in the machining area. The method used in this research is Block Layout Overview with Computerized Planning using Logic and Algorithm (Blocplan). The results showed that the redesign of the machining area could reduce stagnation by adding 1 unit of multi drill machine. Relayout in the machining area can reduce 93” time stagnation for the K2SA rear ABS type which can produce 2 outputs at once. The delay in the machining area can be reduced from 4,863 seconds to 0 seconds.
重新设计布局,以消除停滞使用块计划,以提高生产效率
随着汽车工业的快速发展,子公司也随之增长。其中一家子公司是生产车轮等汽车零部件的公司。2021年的销量增加到200多万件,而2022年至4月的销量超过了100万件。由于生产能力不足,无法满足高需求,其中之一是加工领域。本研究旨在通过重新设计工厂的布局来提高效率,这被认为是增加加工区域的生产结果。本研究使用的方法是使用逻辑和算法的计算机化规划的块布局概述(Blocplan)。结果表明,通过对加工区域的重新设计,增加1台多台钻床,可以减少停滞现象。在加工区域的布局可以减少93“时间停滞的K2SA后ABS类型,可以一次产生2个输出。加工区域的延迟可从4863秒减少到0秒。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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审稿时长
12 weeks
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