Remediation of Oil Production by Matrix Acidizing Method on an Oil Well

Njeudjang Kasi, Yandjimaing Justine, Nitcheu Madeleine, N. Theophile
{"title":"Remediation of Oil Production by Matrix Acidizing Method on an Oil Well","authors":"Njeudjang Kasi, Yandjimaing Justine, Nitcheu Madeleine, N. Theophile","doi":"10.31699/ijcpe.2022.4.1","DOIUrl":null,"url":null,"abstract":"   The remediation oil production by matrix acidizing method on the well named \"X\" (for confidential reasons) is scrutinized in this paper. Initial production of 1150 bpd, production index of 2.8 STB/Psi/d and permeability of 150md, in 2018 two years down the lane this dropped to 450 bpd, production index 0.7 STB/Psi/d. The declined observed on the production index is trouble shouted and after elimination of (no completion damage/perforation damage), the skin is calculated by carrying out a well test (build-up test) whose extrapolation in excel over times gave us a skin of 40.The reservoir heterogeneity, containing >20% of feldspar, carbonates and paraffin’s guided thematrix acidizing design and treatment proposition to remedy this problem. A positive displacement pump (HT400), boosted by a centrifugal pump were used to pump the acid treatment through high pressure treating line downhole. Halliburton insite for stimulation the (IFS) software monitored treating pressure and surface flow rate, keeping injection rate below fracturing pressure. PipeSim software is used to run the nodal analysis before and after treatment this helped to forecast optimal production rates and pressure after treatments. Matrix acidizing method applied on the well X increased the production to 850 bpd with production index of 2 STD/psi/d, skin - 1.5. The economic benefit to the company stood at (profit oil 21,699,500 USD.) over a two years period of production. Meanwhile uncertainties in demand and supply of crude oil at the international market cause constant fluctuation in oil prices, this should be strongly considered upon execution of this project. Overall applications of this acidizing treatment can be carried out on reservoirs with similar mineralogy. HCl/HF blend dissolves sandstone, mud stone and calcite minerals thus reservoir porosity and permeability can be enhanced in regions extending several meters around the injection well.  ","PeriodicalId":53067,"journal":{"name":"Iraqi Journal of Chemical and Petroleum Engineering","volume":" ","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2022-12-30","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"1","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"Iraqi Journal of Chemical and Petroleum Engineering","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.31699/ijcpe.2022.4.1","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 1

Abstract

   The remediation oil production by matrix acidizing method on the well named "X" (for confidential reasons) is scrutinized in this paper. Initial production of 1150 bpd, production index of 2.8 STB/Psi/d and permeability of 150md, in 2018 two years down the lane this dropped to 450 bpd, production index 0.7 STB/Psi/d. The declined observed on the production index is trouble shouted and after elimination of (no completion damage/perforation damage), the skin is calculated by carrying out a well test (build-up test) whose extrapolation in excel over times gave us a skin of 40.The reservoir heterogeneity, containing >20% of feldspar, carbonates and paraffin’s guided thematrix acidizing design and treatment proposition to remedy this problem. A positive displacement pump (HT400), boosted by a centrifugal pump were used to pump the acid treatment through high pressure treating line downhole. Halliburton insite for stimulation the (IFS) software monitored treating pressure and surface flow rate, keeping injection rate below fracturing pressure. PipeSim software is used to run the nodal analysis before and after treatment this helped to forecast optimal production rates and pressure after treatments. Matrix acidizing method applied on the well X increased the production to 850 bpd with production index of 2 STD/psi/d, skin - 1.5. The economic benefit to the company stood at (profit oil 21,699,500 USD.) over a two years period of production. Meanwhile uncertainties in demand and supply of crude oil at the international market cause constant fluctuation in oil prices, this should be strongly considered upon execution of this project. Overall applications of this acidizing treatment can be carried out on reservoirs with similar mineralogy. HCl/HF blend dissolves sandstone, mud stone and calcite minerals thus reservoir porosity and permeability can be enhanced in regions extending several meters around the injection well.  
利用基质酸化法对某油井进行采油修复
本文对X井(保密)基质酸化法修复采油进行了详细研究。最初的产量为1150桶/天,生产指数为2.8 STB/Psi/d,渗透率为150md,在2018年,这一数字下降到450桶/天,生产指数为0.7 STB/Psi/d。在生产指数上观察到的下降是有问题的,在消除(没有完井损伤/射孔损伤)之后,通过进行试井(建井测试)来计算表皮,该测试的外推结果是40。储层的非均质性(含长石、碳酸盐和石蜡)指导了基质酸化设计和处理建议,以解决这一问题。在离心泵的推动下,采用容积泵(HT400)将酸处理液泵入井下高压处理管线。哈里伯顿在增产作业现场使用IFS软件监测处理压力和地面流量,使注入速度保持在压裂压力以下。使用PipeSim软件在处理前后进行节点分析,这有助于预测处理后的最佳产量和压力。X井采用基质酸化方法,产量提高到850桶/天,产量指数为2 STD/psi/d,表皮为- 1.5。在两年的生产期间,公司的经济效益为21,699,500美元。同时,国际市场原油供需的不确定性导致油价不断波动,在实施本项目时应充分考虑这一点。这种酸化处理的总体应用可以在具有相似矿物学的储层上进行。HCl/HF混合物溶解了砂岩、泥石和方解石矿物,因此在注入井周围延伸数米的区域可以提高储层的孔隙度和渗透率。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
求助全文
约1分钟内获得全文 求助全文
来源期刊
自引率
0.00%
发文量
26
审稿时长
12 weeks
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
确定
请完成安全验证×
copy
已复制链接
快去分享给好友吧!
我知道了
右上角分享
点击右上角分享
0
联系我们:info@booksci.cn Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。 Copyright © 2023 布克学术 All rights reserved.
京ICP备2023020795号-1
ghs 京公网安备 11010802042870号
Book学术文献互助
Book学术文献互助群
群 号:604180095
Book学术官方微信