Perbandingan Efisiensi Aktual Dan Spesifikasi Generator BTG II Power Plant PT. Semen Tonasa 2×35 MW Pada Berbagai Beban Aktual

U. Usman, A. Multazam, A. Gaffar
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Abstract

The efficiency of generators in a power plant decreases as running duration increases. This can also happen to the generator of the PT. Steam Power Plant. The Semen Tonasa Power Plant is also known as the Boiler Turbine Generator (BTG) Power Plant. BTG II has been operating for approximately 8 years and based on generator operation data, there has been a decrease in the power generated by the genera-tor, when viewed from the power input to the current turbine, compared to the initial operation of this plant. The aims of this study are to assess the value of the real generator efficiency and compare it to the efficiency generator based on its specifications. Data loading is required to ascertain the true value of generator efficiency, as the output power created by the generator and the input power is the power gen-erated by the turbine, which is computed using the enthalpy reduction method. According to the research, the average generator efficiency values for generator units C and D are 91.36 percent and 90.34 percent, respectively, with real average loads of 25,56 MW and 25,08 MW. In comparison to the data standards, generator unit C saw a 6.76 percent drop in efficiency, whereas generator unit D experienced a 7.76 per-cent decrease efficiency. Comparison with the data specifications for generator units C experienced a decrease in efficiency of 6,76% while generator unit D experienced a decrease in efficiency of 7,76%. The efficiency of the generator in unit C decreased 0.85% per year, and unit D was 0.97%.
比较实际的效率和发电机规格比特币II Tonasa水泥发电厂PT . 2×35兆瓦的各种实际负担
发电厂中发电机的效率随着运行时间的增加而降低。这种情况也可能发生在PT蒸汽发电厂的发电机上。Semen Tonasa发电厂也被称为锅炉-涡轮发电机(BTG)发电厂。BTG II已经运行了大约8年,根据发电机运行数据,与该工厂的初始运行相比,从当前涡轮机的功率输入来看,发电机的发电量有所下降。本研究的目的是评估实际发电机效率的值,并根据其规格将其与效率发电机进行比较。需要数据加载来确定发电机效率的真实值,因为发电机产生的输出功率和输入功率是涡轮机产生的功率,这是使用焓降法计算的。根据研究,发电机组C和D的平均发电机效率值分别为91.36%和90.34%,实际平均负荷分别为25,56MW和25,08MW。与数据标准相比,发电机组B的效率下降了6.76%,而发电机组D的效率下降7.76%。与数据规范相比,发电机组C的效率下降了6,76%,而发电机组D的效率下降为7,76%。C机组的发电机效率每年下降0.85%,D机组为0.97%。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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