THE APPLICATION OF SIX SIGMA-DMAIC METHOD TO REDUCE DEFECTS AND IMPROVE THE CARTRIDGE CASE PROCESS IN AMMUNITION COMPANY

Merlina Fitri Anggamawarti, P. Pratikto, Y. Sumantri
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Abstract

PT. Pindad has a superior product, namely the 5.56 mm ammunition MU5-TJ. The product performance and quality, to be better, need changes in manufacturing processes and stricter quality control. In the MU5-TJ manufacturing process, defects in the cartridge significantly contribute to defective products, reaching 48.6%. This study aimed to evaluate the causes of the defects and improve the quality of the MU5-TJ cartridge production line. The method used in this study was Six Sigma-DMAIC (Define, Measure, Analyze, Improve, Control). The quality identification showed that the gauging process contributes to 67.8% of total defects in all production lines of cartridges. The critical factors were inspection methods and machine settings. Improvements were made by implementing auto-control every 15 minutes by the operators, setting the heading and necking, edge turning, and gauging machine speed. The improvements were shown to increase the sigma level from 3.24 to 3.45 and save the cost by IDR62.372.824,00.
六西格玛DMAIC方法在弹药公司减少缺陷改进弹壳工艺中的应用
平达公司有一种更好的产品,即5.56毫米弹药MU5-TJ。产品的性能和质量要更好,就需要改变生产工艺,加强质量控制。在MU5-TJ制造过程中,墨盒缺陷对不良产品的贡献很大,达到48.6%。本研究旨在评价MU5-TJ墨盒生产线缺陷产生的原因,提高其生产质量。本研究使用的方法是六西格玛- dmaic(定义、测量、分析、改进、控制)。质量鉴定表明,在所有墨盒生产线中,测量过程的缺陷占总缺陷的67.8%。关键因素是检查方法和机器设置。通过每15分钟由操作员进行自动控制,设置头颈、翻边和测量机器速度,进行了改进。结果表明,改进后的西格玛水平从3.24提高到3.45,节约成本62.372.82.4万印尼盾。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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