Experimental Behaviour of Tensioner for Rigid Hangers of Arch Bridges

Q2 Engineering
Designs Pub Date : 2024-06-05 DOI:10.3390/designs8030055
M. Granata, Benedetta Fontana, Marco Rosone, Giovanni Culotta
{"title":"Experimental Behaviour of Tensioner for Rigid Hangers of Arch Bridges","authors":"M. Granata, Benedetta Fontana, Marco Rosone, Giovanni Culotta","doi":"10.3390/designs8030055","DOIUrl":null,"url":null,"abstract":"In steel tied arch bridges where the hangers are made of rigid bars, the replacement of damaged hangers is rather complex. In fact, while generally the cable hangers are already prepared with anchors at the ends and their replacement traces the initial stages of construction with their prestressing, on the contrary, the rigid bars are welded to the arch and the deck, so their replacement must include the design of a new suspension system that allows the insertion of a pretension where this had never been considered. To check the reliability of this new system, a prototype of tensioner was studied for the case of a steel arch bridge in which the high level of corrosion made it necessary to replace all the original hangers with new ones. This entailed the need to test the tensioner performance with the aim of ensuring the axial force transmission between the two hanger segments without slippage in the threads, as well as to test the correct tension setting before construction and putting into service the hangers to be replaced. For this reason, a predictive experimental campaign was carried out on a prototype by means of tests for the mechanical characterization of the materials used, tensile tests of the system, and tensioning tests under load, measuring the displacements and strains of the system elements. The results of the tests, with slippage in the threads limited to the 2% of total elongation, and the turnaround-stressing curves were useful for the definition of the pieces to be assembled during on-site work and for addressing the operating procedures of the tensioning phases on-site during hanger replacement. Validation with the on-site monitoring of stressing operation was conducted at the end; the monitoring of tension through dynamic tests confirmed the agreement of on-site results with the predictive loading tests of the experimental campaign on the tensioner prototype.","PeriodicalId":53150,"journal":{"name":"Designs","volume":"339 3","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2024-06-05","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"Designs","FirstCategoryId":"1094","ListUrlMain":"https://doi.org/10.3390/designs8030055","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"Q2","JCRName":"Engineering","Score":null,"Total":0}
引用次数: 0

Abstract

In steel tied arch bridges where the hangers are made of rigid bars, the replacement of damaged hangers is rather complex. In fact, while generally the cable hangers are already prepared with anchors at the ends and their replacement traces the initial stages of construction with their prestressing, on the contrary, the rigid bars are welded to the arch and the deck, so their replacement must include the design of a new suspension system that allows the insertion of a pretension where this had never been considered. To check the reliability of this new system, a prototype of tensioner was studied for the case of a steel arch bridge in which the high level of corrosion made it necessary to replace all the original hangers with new ones. This entailed the need to test the tensioner performance with the aim of ensuring the axial force transmission between the two hanger segments without slippage in the threads, as well as to test the correct tension setting before construction and putting into service the hangers to be replaced. For this reason, a predictive experimental campaign was carried out on a prototype by means of tests for the mechanical characterization of the materials used, tensile tests of the system, and tensioning tests under load, measuring the displacements and strains of the system elements. The results of the tests, with slippage in the threads limited to the 2% of total elongation, and the turnaround-stressing curves were useful for the definition of the pieces to be assembled during on-site work and for addressing the operating procedures of the tensioning phases on-site during hanger replacement. Validation with the on-site monitoring of stressing operation was conducted at the end; the monitoring of tension through dynamic tests confirmed the agreement of on-site results with the predictive loading tests of the experimental campaign on the tensioner prototype.
拱桥刚性吊架拉伸器的实验行为
在钢系杆拱桥中,吊架是由刚性杆件制成的,损坏吊架的更换相当复杂。事实上,一般情况下,缆索吊架的两端已经准备好了锚栓,在施工初期就可以通过预应力对其进行更换,相反,刚性钢筋是焊接在拱桥和桥面上的,因此更换时必须设计一种新的悬挂系统,以便在从未考虑过的地方插入预应力。为了检验这一新系统的可靠性,我们以一座钢拱桥为例,对拉伸器原型进行了研究。这就需要对拉伸器的性能进行测试,以确保两个支吊架之间的轴向力传递不会在螺纹中出现滑动,并在施工和将要更换的支吊架投入使用之前测试正确的张力设置。为此,对原型进行了预测性实验,包括所用材料的机械特性测试、系统拉伸测试和负载下的张力测试,测量系统元件的位移和应变。测试结果(螺纹的滑移量限制在总伸长量的 2%)和周转-应力曲线有助于确定现场工作中的组装件,也有助于解决更换吊架时现场拉伸阶段的操作程序问题。最后,通过现场监测应力操作进行了验证;通过动态测试对张力进行监测,证实了现场结果与拉伸器原型实验活动的预测加载测试结果一致。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
求助全文
约1分钟内获得全文 求助全文
来源期刊
Designs
Designs Engineering-Engineering (miscellaneous)
CiteScore
3.90
自引率
0.00%
发文量
0
审稿时长
11 weeks
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
确定
请完成安全验证×
copy
已复制链接
快去分享给好友吧!
我知道了
右上角分享
点击右上角分享
0
联系我们:info@booksci.cn Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。 Copyright © 2023 布克学术 All rights reserved.
京ICP备2023020795号-1
ghs 京公网安备 11010802042870号
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术官方微信