Analysis of Power Transformer Insulation: A Case Study in 150 kV Bantul Substation

A. Hidayat, Agus Jamal, A. N. N. Chamim, R. Syahputra, Jeckson Jeckson
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引用次数: 1

Abstract

Insulation of the transformer is one of the essential components. So that the quality of the resistance in the isolation of the transformer is essential to note the condition, in order to find out the condition of the transformer isolation, several tests must be performed, namely the polarization index, delta tangent, and break down voltage. In this study, all three tests were carried out on Transformer 1 in the 150 kV Bantul substation. Polarization index testing itself is testing the leakage current on the transformer isolation by comparing the test results for 1 minute with the results of the 10-minute drive test. While delta tangent is testing capacitive leakage current in the isolation transformer, and break down voltage is a test of the ability of the breakdown voltage in transformer insulation oil. Based on the results of the analysis, it can be seen that the value of the transformer polarization index in 2016 and 2018, the average value between the windings has been in the rating of 1.25-2.0. As for the delta tangent test results in 2016 and 2018, the value between the capacitive parts is already in the rating of 0.18% -0.36%. For the breakdown voltage test results in 2016 and 2018, the average breakdown voltage value is 43.9 kV/mm - 65.5 kV/mm. From these data, it can be concluded that the transformer isolation conditions in 2016 and 2018 are in good condition, although there was a decline in the transformer isolation conditions in 2016. However, the National Electric Company has made repairs and maintenance of the isolation transformer. This is seen due to an increase in the quality of transformer insulation in 2018. Repair and maintenance of transformer insulation are done to maximize the work system and the life of the transformer.
电力变压器绝缘分析——以150kv班图尔变电站为例
变压器的绝缘是必不可少的部件之一。所以说变压器在隔离状态下电阻的质量是必须要注意的,为了找出变压器隔离状态,必须进行几项试验,即极化指数、δ正切、击穿电压。在本研究中,这三项试验都是在Bantul变电站的150 kV变压器1上进行的。极化指数测试本身就是通过比较1分钟的测试结果和10分钟的驱动测试结果来测试变压器隔离上的泄漏电流。而正切是测试隔离变压器中的电容漏电流,击穿电压是测试变压器绝缘油中击穿电压的能力。根据分析结果可以看出,2016年和2018年变压器极化指数的数值,绕组之间的平均值一直在1.25-2.0的额定值之间。对于2016年和2018年的delta tan测试结果,电容部分之间的值已经在0.18% -0.36%的额定值范围内。2016年和2018年击穿电压试验结果平均击穿电压值为43.9 kV/mm ~ 65.5 kV/mm。从这些数据可以得出结论,2016年和2018年的变压器隔离条件都处于良好状态,尽管2016年变压器隔离条件有所下降。不过,国家电力公司对隔离变压器进行了维修和保养。这是由于2018年变压器绝缘质量的提高。变压器绝缘的维修和保养是为了最大限度地提高变压器的工作系统和使用寿命。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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