Elevating Drilling Performance & Efficiency to Highest Levels in Field A–Journey from 150 to 31 Drilling Days.

S. Ullah, Muhammad Sajjad Ashraf, Ali Mohiuddin Ahmed, Daniyal Ahmad, Mohammad Murad Haider, Mohammad Mohsin Usmani, Syed Dost Ali
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Abstract

Field A is one of the most challenging fields in the Potowar region of Northern Pakistan with severe problems of fluid loss, high-pressure shallow water influx, low drillability, clay reactivity/ shale instability and depleted reservoir sections. This paper gives a brief overview of the methods and changes made along with results achieved, enabling the well to reach total depth in just 31 days compared to an average of 150 days taken on offset wells. Due to severe drilling challenges, the wells were drilled in six-hole sections starting with 36" surface hole. An entirely new well engineering strategy has been utilized to enhance the drilling performance in the last five wells drilled in the field. Some of the major areas of change include Customized bit design, BHA and hydraulics design, casing design optimization and change in casing seat strategy as well as novel changes in drilling fluid design and selection of Loss Control Material. Dysfunctions and limiters in drilling which were affecting the hole cleaning, mechanical specific energy (MSE), hydraulics efficiency, and ROP were eliminated. A detailed analysis of the impact of changes in bits and bottom hole assembly design, drilling fluids design, and casing design is shared in the study for the last fifteen wells drilled in the field. Continuous learning and enhancements in all the subject areas are analyzed with respect to the use of different strategies and technologies. An analysis has been performed for non-productive time, its root cause and successful actions taken to reduce its occurrence. A huge reduction in drilling time, cost and risks have been achieved as a result of mentioned changes in the latest well setting a benchmark in the entire region. Dry hole time for the last well has been reduced by 78 %, while 65% cost reduction is achieved as compared to the previous average time and cost respectively. After removing the dysfunctions / limiters; ROP enhancement of 5 to 10 times has been achieved in different hole sections. The learning and experience from the use of discussed technologies and drilling practices can be helpful for optimizing challenging wells with the problems of pressure reversals, drilling fluids losses, well control, drillability issues in gumbo clay/ shales and wellbore stability.
将油田a段的钻井性能和效率从150天提高到31天,达到最高水平。
A油田是巴基斯坦北部Potowar地区最具挑战性的油田之一,存在严重的流体漏失、高压浅水涌入、可钻性低、粘土反应性/页岩不稳定以及油藏段枯竭等问题。本文简要介绍了这些方法和所做的改变以及取得的成果,使该井在31天内达到总深度,而邻井平均需要150天。由于严峻的钻井挑战,这些井从36英寸的地面井眼开始钻成6孔段。在该油田的最后5口井中,采用了一种全新的钻井工程策略来提高钻井性能。一些主要的变化领域包括定制钻头设计、BHA和液压设计、套管设计优化和套管座策略的变化,以及钻井液设计和防漏失材料选择的新变化。消除了钻井过程中影响井眼清洁、机械比能(MSE)、水力效率和ROP的功能障碍和限制因素。在该油田最后15口井的研究中,详细分析了钻头和井底组合设计、钻井液设计和套管设计变化的影响。根据不同策略和技术的使用,分析了所有主题领域的持续学习和改进。对非生产时间进行了分析,分析了非生产时间的根本原因,并采取了成功的措施来减少非生产时间的发生。由于上述最新井的变化,钻井时间、成本和风险大幅减少,成为整个地区的基准。与之前的平均时间和成本相比,最后一口井的干井时间减少了78%,成本降低了65%。去除功能障碍/限制因素后;不同井段的机械钻速提高了5 ~ 10倍。通过使用所讨论的技术和钻井实践的学习和经验,可以帮助优化具有挑战性的井,解决压力逆转、钻井液漏失、井控、gumbo粘土/页岩的可钻性问题和井眼稳定性问题。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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