Implementation of Lean Manufacturing to Improve Air Handling Unit Coil Manufacturing in Saudi Air Conditioning Manufacturing Company (SAMCO)

Salman A. Alsayed
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Abstract

This report aims to improve the production operations of the coils shop of air handling units (AHU) at Saudi Air Conditioning Manufacturing Company (SAMCO) by applying lean manufacturing strategy. The coils shop of AHU experienced several issues which impact negatively on its performance and increase the non-added values. For instance, it suffers from significant amount of scrap, low machines utilization, extra manpower, long machine set up time, and the absence of process safety system. In this report, the required data were collected by three ways; observation, recording and conducting the interviews with the related people. These data were analyzed by a wide range of tools, which are used to apply lean manufacturing such as, value stream mapping, 5S, work standardized, manual handling assessment chart, snook table, one-dimensional cutting optimizer, and mistake proofing. As a result, a significant reduction in the overall cost of coils shops production processes were obtained. For instance, the average machines set up time was reduced by 18 %, number of set up per shift was reduced by 20.8 %, the number of operators was reduced by 26.3 %, the quality of the product was increased and the safety of the processes was enhanced. It is worthy to note the amount of the scrap was dropped by approximately 71 %.
沙特空调制造公司(SAMCO)实施精益制造改进空气处理机组盘管制造
本报告旨在通过应用精益生产战略,改善沙特空调制造公司(SAMCO)空气处理机组(AHU)盘管车间的生产运营。AHU的盘管车间经历了几个问题,这些问题对其性能产生了负面影响,并增加了非附加值。例如,废钢量大,机器利用率低,需要额外的人力,机器设置时间长,缺乏过程安全系统。在本报告中,通过三种方式收集所需的数据;对相关人员进行观察、记录和访谈。这些数据通过价值流图、5S、作业标准化、手工处理评估图、snook表、一维切割优化器、防错等广泛的工具进行分析,用于精益制造的应用。结果,线圈车间生产过程的总成本显著降低。例如,平均机器设置时间减少了18%,每班设置次数减少了20.8%,操作人员减少了26.3%,提高了产品质量,增强了过程的安全性。值得注意的是,废料的数量下降了大约71%。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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