TUBING HANGER INVESTIGATION OF LOADING

Zenfira Huseynli Zenfira Huseynli, Alieva Rovshana Alieva Rovshana, Akbar Hashimov Akbar Hashimov
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Abstract

In this article, the failures of tube hangers made from UNS N07718 are discussed. An arrangement known as a tubing hanger may be found in wells that produce either oil or gas. It is positioned in the upper tubing head’s bowl after it has been installed. The tubing is held in place by this, and a main annulus seal is created between tubing also the production casing. This holds the tubing in place, and at the same time, it creates a primary annulus seal between tubing also production casing. When compared to odd component in wellhead system, tubing hangers are available in a broader range of styles and sizes than any other option. Tubing hangers made of UNS N07718 are often used in the installation process of sour service oil and gas wells that operate under high pressure and also high temperatures. Afterwards more than 10 years of service, it was only recently found that the tubing hanger made of UNS N07718 had failed in sour wells. Failures of the tubing hanger will inference in substantial production delays as well as high workover expenses. The purpose of this research is to demonstrate the failure mechanism of tubing hanger furthermore its ramifications on existing wells that were erected with material that is comparable to what was used here. In order to establish what caused the failure, each and every exposure that was brought on by well intervention efforts was evaluated. The manner of failure of stringer head suspension was researched, as was its influence on already existing wells that had been erected with materials that were comparable. Keywords: tubing head, tubing hanger, tubing thread, back pressure valve profile, landing shoulder, snap ring, running thread,
油管悬挂器载荷调查
本文讨论了UNS N07718管吊架的失效问题。在产油或产气的井中可以找到一种称为油管悬挂器的装置。安装后,将其放置在上油管头的碗中。油管被固定在适当的位置,在油管和生产套管之间形成一个主环空密封。这样可以固定油管,同时在油管和生产套管之间形成初级环空密封。与井口系统中的其他部件相比,油管悬挂器的样式和尺寸范围更广。由UNS N07718制成的油管悬挂器经常用于高压和高温下的含酸油气井的安装过程中。经过10多年的使用,直到最近才发现UNS N07718制成的油管悬挂器在含酸井中失效。油管悬挂器的故障将导致大量的生产延迟和高修井费用。本研究的目的是证明油管悬挂器的失效机制,以及它对现有井的影响,这些井是用与这里使用的材料相当的材料建造的。为了确定导致故障的原因,对修井作业带来的每一次暴露都进行了评估。研究了弦杆封头悬吊的失效方式,以及它对使用类似材料建造的现有井的影响。关键词:油管头、油管悬挂器、油管螺纹、背压阀型线、着陆肩、卡环、下入螺纹、
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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