Tailored Engineering Cementing Solution to Maintain Well Integrity in Shallowest Liner for Underground Gas Storage Project - Case History from Southwest China

Fangfang Li, Devesh Bhaisora, Huang Yue
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Abstract

Underground gas storage (UGS) wells have emerged as a strategic solution in China. Success of UGS projects largely depends upon maintaining long term well integrity. Cement slurries that are placed across a wellbore should exhibit superior cement bonding as evidenced through a cement bond log (CBL) and long-term integrity to sustain the cyclic stress change by the injection and production process. Such slurries should have improved mechanical properties and the job execution should follow all cementing best practices. The well architecture included a 9 5/8-in. surface casing and a 7-in. production liner. The 7-in. Liner was run inside an 8.5-in. open hole and extended to surface using a tie-back liner. This well architecture should have a superior quality of cement across the entire liner. Multiple Finite Element Analysis (FEA) runs were performed to determine an optimum Young's modulus and Poisson Ratio for the cement slurry. These rigorous tests can take weeks to complete. As the well was shallow, to cover a wide range of well profiles, three different slurries were tested prior to the job. The initial mud weight planned for the well was in the range of 1.25 g/cm3 to 1.4 g/cm3. Due to gas influx, the mud density in the section was increased to 1.90 g/cm3. However, losses were also encountered at this mud density. Hydraulic modelling was revised, and slurry rheology and pumping rates were optimized to ensure equivalent circulation density (ECD) control within the pore pressure and fracture gradient window. Displacement rates were optimized to facilitate good displacement efficiency for hole cleaning. The slurry design was tailored with special additives to provide a synergetic effect of improving mechanical properties and minimizing seepage losses. Multiple computational fluid dynamics (CFD) runs were performed to evaluate the cementing job quality and based on the simulations it was decided to increase the cement volume to minimize any impact of contamination. The cementing job was performed with no operational issues and cement returns were observed above the top of the liner. Two different cement evaluation logs - CBL and ultra-sonic log, were conducted and showed good cement quality in the open hole section, meeting the well objectives. With this successful implementation, the tailored engineered cementing solution was highly recognized. The design and execution methodology were highlighted as the guideline for further successful cementing operations in UGS projects. This study shows a fully comprehensive and scientific way to improve cementing quality for long-term well integrity for UGS projects.
为地下储气库项目量身定制的工程固井解决方案,以保持最浅尾管井的完整性-中国西南地区的历史案例
地下储气井(UGS)已成为中国的战略解决方案。UGS项目的成功在很大程度上取决于能否长期保持井的完整性。通过水泥胶结测井(CBL)和长期完整性来证明,在注入和生产过程中,放置在井眼上的水泥浆应具有良好的水泥胶结性,以维持循环应力变化。这种浆液应具有更好的机械性能,作业执行应遵循所有固井最佳实践。井的结构包括一个9 5/8-in。地面套管和7英寸套管。生产衬。7英寸。尾管下入8.5英寸套管。裸眼并使用回接尾管延伸至地面。这种井的结构应该在整个尾管中使用高质量的水泥。进行了多次有限元分析(FEA),以确定水泥浆的最佳杨氏模量和泊松比。这些严格的测试可能需要数周才能完成。由于该井较浅,为了覆盖更大范围的井剖面,作业前测试了三种不同的泥浆。该井的初始泥浆密度计划在1.25 g/cm3至1.4 g/cm3之间。由于气侵,该段泥浆密度增加到1.90 g/cm3。然而,在这种泥浆密度下也会遇到漏失。修正了水力模型,优化了泥浆流变学和泵送速率,以确保在孔隙压力和裂缝梯度窗口内控制等效循环密度(ECD)。为了提高井眼清洗效率,对驱替速率进行了优化。泥浆的设计中加入了特殊的添加剂,以提供改善机械性能和减少渗透损失的协同效应。为了评估固井作业质量,进行了多次计算流体动力学(CFD)测试,根据模拟结果,决定增加固井体积,以尽量减少污染的影响。固井作业没有出现任何操作问题,尾管顶部的固井情况良好。两种不同的水泥评价测井- CBL和超声波测井-均显示了裸眼段的水泥质量良好,达到了井的目标。通过此次成功实施,定制工程固井解决方案得到了高度认可。设计和执行方法被强调为UGS项目中进一步成功固井作业的指导方针。该研究为UGS项目提供了一条全面、科学的提高固井质量、保证油井长期完整性的途径。
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