Analisa Pemasangan UPS VFD LFO Feeder Untuk Mengantisipasi Gangguan Eksternal

Dikse Pancane, Angling Kameswara, Gede Adrama
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Abstract

On July 1 and July 26 2017 there was a simultaneous trip of PLTDG Units 1,2,5,5,6,7,8 and PLTDG Units 1,3,4,5,6,7,8,9 due to a momentary drop voltage due to disturbance kites on the 150 KV line network sanur – gianyar. From the trip conditions, it shows that there is a problem with the generator unit equipment which causes PLTDG units 1,2,3,4,5,6,7,8,9 to trip due to a momentary drop voltage. From the results of the analysis, it is known that the unit trip was caused by a trip on the Pht Line 150 KV to the ship - Padang sambian on the Padang sambian side which resulted in a drop voltage on the low voltage side of 280.4 V or 29.9%. from Unominal. The trip limit of 200MW low-voltage PLTDG according to technical data is 351V or 12.3% of Unominal. The best option to solve the drop voltage fault solution is to install a 10KVA UPS on the LFO feeder pump power supply. The difference before and after the installation of the UPS feeder LFO is that before the installation of the low voltage UPS it drops to 280.4 V or 29.9% of Unominal, and the machine load drops to 11.6 MW. For the results after UPS installation there is no drop voltage value on the low voltage side which means that the UPS installation is successful as a voltage drop solution. So that the difference is obtained on the low voltage side of 119.6 V and on the engine load of 5 MW. Thus, the implementation of a UPS installation on a 200MW PLTDG is very important, in addition to supporting the reliability of the generator system and speeding up recovery in the event of a drop voltage, it can also be economically profitable, so that the company does not lose when the generating unit trips.
分析安装UPS VFD LFO馈程以预测外部干扰
2017年7月1日和7月26日,由于sanur - gianyar 150 KV线路网络上的干扰风筝造成瞬间电压下降,PLTDG 1、2、5、5、6、7、8、8号机组和PLTDG 1、3、4、5、6、7、8、9号机组同时跳闸。从跳闸情况来看,发电机组设备存在问题,导致PLTDG机组1、2、3、4、5、6、7、8、9因瞬间电压下降而跳闸。从分析结果可知,机组跳闸是由于150 KV Pht线在Padang sambian一侧对船- Padang sambian进行跳闸,导致低压侧电压下降280.4 V或29.9%。从Unominal。根据技术数据200MW低压PLTDG的跳闸限值为351V,即米纳尔的12.3%。解决降压故障的最佳方案是在LFO给料泵电源上安装10KVA UPS。UPS馈线LFO安装前后的不同之处在于,低压UPS安装前降至280.4 V或乌米纳尔的29.9%,机器负载降至11.6 MW。如果UPS安装完成后,低压侧无电压降值,说明UPS安装成功,解决电压降问题。因此,在119.6 V的低压侧和5 MW的发动机负载上获得了差值。因此,在200MW的PLTDG上安装UPS是非常重要的,除了支持发电机系统的可靠性和在电压下降的情况下加速恢复之外,它还可以在经济上获利,这样当发电机组跳闸时公司就不会损失。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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