Reduction in Roll Wear Through Technological Interventions at CRM & SSM of Rourkela Steel Plant

S. Thakur, S. K. Mohapatra, P. Pathak, D. Roy, C. Mishra
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Abstract

Cold Rolling Mill (CRM) complex of Rourkela Steel Plant (RSP) was set up in 1968. The CRM has two pickling lines which use sulphuric acid as pickling medium. Under-pickling is inherent problem with sulphuric acid pickling line. Under-pickled coils processed at tandem mill leads to contamination of emulsion leading to increased roll wear and poor surface quality of cold rolled coils. Also, the deficient roll cooling system aggravates the situation, leading to higher occurrence of strip breakage and inferior shape of the coils. Technological measures were taken both at the Pickling Line and at the Tandem Mill to improve their operating conditions. These measures include introduction of improved scale washing system at Pickling Line and heat exchanger in acid regeneration plant to improve pickling bath condition. New generation ‘tantalum shell and tube heat exchanger’ introduced in pickling lines to reduce the under-pickling. Roll cooling system at Tandem Mill was modified to reduce thermal- crown of work rolls, which helped in reduction in roll wear by 20%. With these measures, diversion of CR coils due to bad shape reduce by 30%.

Electrical grade of steel produced at Silicon Steel Mill (SSM) is one of the major revenue- earners for RSP. Electrical steel is cold rolled in four high cold reversing mill at SSM. The thermal crown of the work rolls in the mill found to be high, leading to higher specific roll consumption, lower campaign size and poor surface quality of electrical steel rolled in this mill. A modified roll cooling system with differential flow density along the work roll barrel in accordance to the roll thermal profile was introduced at reversing mill to improve shape of the cold rolled coils. The headers have been divided into three zones depending on the intensity of the cooling required with the central zone having the highest flow density followed by the intermediate and the end zones. A self-cleaning wedge type auto filter capable of filtration of 300 micron level was introduced for supply of continuous emulsion flow to roll cooling headers. The improved roll cooling system has led to reduction in roll wear and the specific roll consumption has reduced by 20%.
鲁克拉钢厂CRM & SSM技术干预降低轧辊磨损
Rourkela钢厂(RSP)的冷轧厂(CRM)综合体成立于1968年。CRM有两条酸洗线,以硫酸为酸洗介质。酸洗不足是酸洗生产线的固有问题。冷轧带钢在连轧过程中未充分酸洗会导致乳剂污染,导致轧辊磨损增加,冷轧带钢表面质量差。此外,不完善的轧辊冷却系统加剧了这种情况,导致带钢断裂的发生率较高,卷板形状较差。对酸洗线和连轧机的运行状况采取了技术措施。这些措施包括在酸洗生产线引入改进的水垢洗涤系统和在酸再生装置中引入热交换器来改善酸洗槽条件。在酸洗生产线中引入新一代“钽壳管式换热器”,减少酸洗不足。对连轧轧辊冷却系统进行了改进,减少了工作辊的热凸度,使轧辊磨损减少了20%。通过这些措施,由于形状不良导致的CR线圈导流减少了30%。硅钢厂(SSM)生产的电工级钢是RSP的主要收入来源之一。电钢在四高冷可逆轧机上进行冷轧。轧钢工作辊的热凸度高,导致轧钢比耗高,活动尺寸小,轧钢表面质量差。为了改善冷轧卷板的形状,在可逆轧机上采用了一种根据辊热剖面沿工作辊筒流密度变化的轧制冷却系统。根据所需冷却的强度,集管被分为三个区域,中心区域具有最高的流量密度,其次是中间和末端区域。介绍了一种能够过滤300微米级的自清洁楔形自动过滤器,用于连续的乳化液流供给轧辊冷却集管。改进后的轧辊冷却系统减少了轧辊的磨损,轧辊的比耗降低了20%。
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