Total Productive Maintenance (TPM) Implementation to ImproveMachine Efficiency

Novera Elisa Triana, Sakti Aji Lesmana
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Abstract

The company focuses on producing quality products by implementing the Toyota Production System, known as TPS. The current constraint is the absence of maintenance on the Leak Test, thereby reducing production profits caused by high engine damage. This also causes the average repair time for the Leak Test Model 4L45W engine to be above the repair target set by the company, where the company targets an average repair time per month of 12 minutes. For this reason, corrective steps are needed so that the production process runs smoothly according to operational standards. This step involves proposing the implementation of Total Productive Maintenance (TPM). It is known that the average Overall Equipment Effectiveness (OEE) Leak Test machine in June–August was 60.09%. The Japan Institute of Plant Maintenance (JIPM) stipulates that if the OEE value is equal to 60%, it indicates that there is a lot of room for improvement. After implementing Total Productive Maintenance (TPM) on the Leak Testin September, the OEE value rose to 94.33%, and the average monthly repair timemet the company's target of 9.2 minutes. This greatly affects the cost of production due to lower production costs due to overtime. This indicates improvement, and the first step in the proposed implementation of the Total Productive Maintenance Machine Leak Test model 4L45W is said to be successful
实施全面生产维护(TPM)以提高机器效率
该公司通过实施丰田生产系统(TPS),专注于生产优质产品。目前的限制是缺乏对泄漏试验的维护,从而降低了高发动机损坏造成的生产利润。这也导致泄漏测试型号4L45W发动机的平均维修时间高于公司设定的维修目标,公司的目标是每月平均维修时间为12分钟。因此,需要采取纠正措施,使生产过程按照操作标准顺利进行。这一步包括建议实施全面生产维护(TPM)。据了解,6 - 8月整机效率(OEE)检漏机平均为60.09%。日本工厂维修研究所(JIPM)规定,如果OEE值等于60%,则表明有很大的改进空间。在9月的泄漏测试中实施全面生产维护(TPM)后,OEE值上升到94.33%,平均每月维修时间为9.2分钟。这极大地影响了生产成本,因为加班降低了生产成本。这表明改进,并且在建议实施的全面生产性维护机器泄漏测试模型4L45W的第一步据说是成功的
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