Use of ramp test to expedite return to service of damaged stator winding

W. McDermid, R. Gamblin
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引用次数: 6

Abstract

The fracture of a clamping finger resulted in major damage to the stator core and winding of a 13.8 kV 120 MVA hydro generator. Immediately following the fault the fire suppression water deluge system operated for a period of time. The polyester bonded mica insulation system of this stator winding is known to be vulnerable to tape separations in the end arm area. High direct-voltage ramp tests were used on four occasions to: ldr Identify stator coils needing replacement ldr Determine adequacy of hot air drying ldr Determine adequacy of drying under short circuit conditions ldr Monitor subsequent improvement in service The objective was to return the unit to service as quickly as possible in the expectation that the condition of the groundwall insulation would continue to improve. To date this approach has been successful.
使用斜坡试验加速损坏的定子绕组恢复工作
一台13.8 kV 120 MVA水轮发电机的定子铁芯和绕组因夹紧手指断裂而严重损坏。故障发生后,灭火淋水系统随即运行了一段时间。这种定子绕组的聚酯粘结云母绝缘系统在端臂区域易受胶带分离的影响。高直接电压斜坡试验进行了四次,目的是:确定需要更换的定子线圈确定热风干燥是否适当确定短路条件下的干燥是否适当监测后续使用情况的改善情况,目的是在期望地壁绝缘状况继续改善的情况下,尽快使机组恢复使用。迄今为止,这种方法是成功的。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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