Drilling and Cementing to Isolate Productive Series and High Pressure Zones: A Successful Case History Enables Zonal Isolation in High Pressure Gas Well with Close PPFG Margins in South Caspian Basin

Apparao Cherukuri, Elshan Ismayilov, Elgun Zeynalov, Fuad Cabbarov, Vusal Iskandarov, Elkhan Karimov
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Abstract

The objective of this paper is to share the experience of how 7-5/8" section was drilled, and cased-off to enable the zonal isolation in the depleted VII horizon and high-pressure zone with close PPFG margins by managing high risks of differential sticking and loss of circulation at Bulla gas-condensate reservoir which is one of the most complex high-pressure fields with close PPFG margins in the world. The Bulla wells are highly complex wells the Caspian region. Before drilling into the reservoir section which requires high MW, the drilling liner was run to the cased-off VII horizon and high-pressure zone, which have significant challenges such as differential sticking and loss of circulation, previously resulting in stuck pipe and losses. To overcome the challenges, under reaming/liner cementing at MW lower than PP were evaluated and applied to have good cementing across the open hole and good shoe, to drill into the reservoir section in the project. The study helped to identify the issues and actions taken that resulted in significant improvement in well delivery and reduced the risks despite having underbalanced condition during under-reaming/cementing. So is accepting the bitter truth, situation offering limited sets of options was very challenging as having: high risks of differential sticking and loss of circulation due to high MW, high- pressure interval near the setting depth, which required high MW to stabilize the well, need to isolate the high-pressure zone and depleted VII horizon for drilling into the reservoir section. However, the operation plans of managing the ECD within limits by using different MWs, higher MW for running casing and lower MW for UR and cementing have been risk-assessed with all the mitigation, and as a result, the aforementioned intervals were well isolated which was supported by CBL results. No gains or losses were observed during the operations including both casing running and cementing. Finally, having a good cement in the shoe allowed to successfully drill into the reservoir section with high MW accomplishing successful completion of the well without any major problems previously occurring. Therefore, this approach not only reduced the time, cost and also helped to deliver the quality wellbore. The case study of liner cementing at underbalanced conditions provides useful insights of how unconventional techniques can be successfully implemented to achieve the overall accomplishment in well delivery performance.
钻井和固井隔离生产层和高压层:在里海盆地南部PPFG边缘紧密的高压气井中实现了层间隔离的成功案例
本文的目的是分享在Bulla凝析气藏(世界上最复杂的高压油田之一,PPFG裕度很近),如何在枯竭的VII层位和高压层位进行7-5/8”段的钻井和套管封隔的经验,通过管理差压卡钻和循环漏失的高风险,实现层间隔离。Bulla井是里海地区高度复杂的井。在钻进要求高MW的储层段之前,将尾管下至VII套管层位和高压层位,这些层位存在着严重的问题,如差异卡钻和循环漏失,之前会导致卡钻和漏失。为了克服这些挑战,在MW低于PP的情况下,对扩眼/尾管固井进行了评估,并应用于裸眼和鞋部的固井,以钻进项目中的储层段。该研究有助于确定问题和采取的措施,尽管在扩眼/固井过程中存在不平衡状况,但这些措施显著提高了井的交付效率,降低了风险。因此,我们必须接受一个残酷的事实,即提供有限的选择是非常具有挑战性的,因为:由于高MW,在坐封深度附近的高压段,需要高MW来稳定井,需要隔离高压区和枯竭的VII层,以便钻进储层。然而,通过使用不同的MWs(高MW下套管,低MW下UR和固井),在限制范围内管理ECD的作业计划已经进行了风险评估,并进行了所有的缓解措施,结果,上述层段被很好地隔离,这得到了CBL结果的支持。在整个作业过程中,包括套管下入和固井,没有观察到任何收益或损失。最后,由于鞋内固井质量良好,使得该井能够顺利钻进储层段,实现了高MW的完井作业,之前没有出现任何重大问题。因此,这种方法不仅减少了时间和成本,还有助于提供高质量的井眼。欠平衡条件下尾管固井的案例研究为非常规技术的成功实施提供了有用的见解,从而实现了井的整体交付性能。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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