Generator upgrade without stator rewinding

J. Timperley
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引用次数: 1

Abstract

It can be expected that a hydrogenerator stator winding may require replacement when a machine is upgraded more than 25%. A case study is presented where detailed thermal and electrical analysis was performed on spare stator coils purchased when the stator winding of a 158 MVA machine was last rewound in 1988. Results of these accelerated aging tests indicated that continued safe operation of the existing ten-year-old stator coils with an expected turbine upgrade of 27% was possible. Capability tests conducted since the upgrade indicate temperature limitations for the existing insulation system will not be exceeded during normal operation at 200 MVA. Results of thermal and electrical aging tests are presented.
无定子复卷的发电机升级
可以预见,当机器升级超过25%时,水轮发电机定子绕组可能需要更换。本文介绍了一个案例研究,其中详细的热学和电学分析对1988年158 MVA电机定子绕组最后一次重绕时购买的备用定子线圈进行了分析。这些加速老化试验的结果表明,在预期涡轮升级27%的情况下,现有10年的定子线圈继续安全运行是可能的。升级后进行的性能测试表明,在200 MVA的正常运行下,现有绝缘系统的温度限制不会超过。给出了热老化和电老化试验结果。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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