Block-61 Rigless Method for Efficient Permanent Abandonment

Sultan Al Abri, Aala Abbas, M. Jaboob, Muna Al Abri, M. Najwani, S. Al Harrasi, K. Al Fadhli, T. Al Shidhani, A. Al Darai
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Abstract

Well Abandonment is an important stage in the life of any well and in the field development plan in general. Tight regulatory requirements along with high cost made it apparent to search for more innovative methods to design and execute well abandonments more efficiently. Conventionally, well abandonment operations are performed by cementing the wellbore utilizing a drilling rig and its facilities, which is the main driver for the relatively high P&A cost. Here is where the method/initiative of "Rigless abandonment" came into play. This technique replaces the use of drilling rig with other intervention conveyance packages, resulting in a more efficient and cheaper plug and abandonment while satisfying all the regulatory isolation requirements. For a non-standard abandonment operation, the rigless abandonment initiative was a great success. All the abandonment objectives have been met and required barriers have been established while spending 73% of the planned cost only. Despite the challenges faced during the operation, the well abandonment only took 1 day longer than planned. In addition, many lessons learned have been captured to avoid recurrence in the upcoming similar jobs. In the year of 2019, a well in the northern part of bp's block 61 concession was deemed for abandonment due to poor reservoir performance. An opportunity was fore sought by the intervention team to design and execute the required abandonment in a "rigless" style. The planned process considered the use of coiled tubing unit to kill the well and place cement across the targeted Amin formation. Subsequently, utilizing the wireline service to place a plug across the packer before perforating above it. This step was to create a pathway for the cement to communicate between the A-Annulus and the tubing in the wellbore. Then, using the cement unit, the cement was reverse circulate down the annulus and up the tubing. To ensure the placement of the cement, a slickline drift run was conducted after the cement has cured, which indicated TOC at 480 m. Finally, the X-tree was removed, and the tubing and wellhead was cut at surface before performing a top-fill job to cement the remaining void up to surface. The implementation of this abandonment operation also adhered to strict safety standards. The rigid bp safety process guidelines ensured that all challenges and optimization opportunities were fulfilled in a safe manner. The purpose of this paper is to detail how the team pushed the technical envelope to introduce this methodology and share the journey of implementing a cheaper and safer well abandonment alternative.
Block-61无钻机高效永久弃井方法
弃井在任何一口井的生命周期和油田开发计划中都是一个重要阶段。严格的监管要求和高成本使得寻求更创新的方法来更有效地设计和执行弃井作业。通常,弃井作业是通过使用钻井平台及其设施进行固井作业,这是造成P&A成本相对较高的主要原因。这就是“无钻机弃井”方法/倡议发挥作用的地方。该技术取代了钻机与其他修井传输工具的使用,在满足所有监管隔离要求的同时,实现了更高效、更廉价的桥塞和弃井。对于非标准弃井作业,无钻机弃井技术取得了巨大成功。所有弃井目标均已实现,所需障碍已建立,而成本仅为计划成本的73%。尽管在作业过程中面临诸多挑战,但弃井作业只比计划多花了1天时间。此外,吸取了许多经验教训,以避免在即将到来的类似工作中再次发生。2019年,由于储层性能不佳,bp 61区块特许经营权北部的一口井被视为废弃。在此之前,修井团队寻找了一个机会,以“无钻机”的方式设计和执行所需的弃井作业。计划中的过程考虑了使用连续油管装置压井,并在目标Amin地层上固井。随后,在射孔之前,利用电缆服务在封隔器上放置一个桥塞。这一步是为了在a环空和井筒中的油管之间建立一个水泥通道。然后,使用固井装置,将固井沿环空反向循环并沿油管上行。为了确保水泥的位置,在水泥固化后进行了钢丝绳漂移作业,结果表明TOC为480 m。最后,移除X-tree,在地面切割油管和井口,然后进行顶充填作业,将剩余空隙固井至地面。这项弃置作业的实施也遵循严格的安全标准。严格的bp安全流程指南确保所有挑战和优化机会都以安全的方式完成。本文的目的是详细介绍该团队如何推动技术发展,引入这种方法,并分享实施更便宜、更安全的弃井替代方案的过程。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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