Subsea Well Annular Integrity Repair Using Coiled Tubing and Pressure Activated Sealant

J. Johns, Chris Anderson, Juan A. Anguiano, S. Jones
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Abstract

Production from a subsea well was halted due to hurricane activity in the Gulf of Mexico. When the well was returned to production, the annulus experienced a loss of pressure integrity. To achieve regulatory compliance and return the well to production, annular integrity had to be restored in a safe, expeditious manner. This paper will describe the process of operations undertaken to cure this well integrity issue utilizing pressure activated sealant deployed via coiled tubing. Pressure activated sealants have been utilized for a number of years to efficiently cure leaks in a wide variety of applications. One of the first challenges to be addressed when considering a sealant repair is the method of getting the material to the leak site. For the purpose of the subsea well in question, coiled tubing was used to convey the sealant to the sea floor from a service vessel. An ROV then connected the coil to an external tree cap via a flying lead after which the sealant was introduced to the annulus by lube and bleed pressure cycles. The annular integrity issue was analyzed in an effort to determine leak severity and location. Pressure trends noted at annular pressures of 4000 psi indicated a leak ranging from 0.15 – 1.5 lit/min. Gradient analysis indicated that the leak was deep in the completion potentially at a liner lap or the packer. Based on this information a sealant blend approximately 2 ppg heavier than the completion fluid was developed for the purpose of curing the leak. An external tree cap was installed on the well in order to provide access to the annulus of the well via a hot stab connection. About eleven cubic meters of sealant was transferred to the annulus through 2" coiled tubing extended to the sea floor connected to the well via a flying lead. A series of lubricate and bleed cycles were performed to accomplish this without exceeding predetermined pressure limits. After allowing the sealant to settle on the packer, annular pressure was maintained to allow the sealant to cure at the leak site. The pressure differential at the leak caused the liquid sealant to form an elastomeric seal. A positive pressure test was obtained shortly after the process and the well was returned to production. An example of how using pressure activated sealants designed to polymerize only at a leak site affords options to expensive workovers on subsea wells will be provided herein. The use of this technology in concert with coiled tubing deployment represents an expeditious, economic approach to solving complex well integrity issues.
使用连续油管和压力激活密封胶进行海底井环空完整性修复
由于墨西哥湾的飓风活动,海底油井停产。当井重新投入生产时,环空的压力完整性出现了损失。为了符合法规要求并使油井恢复生产,必须以安全、快速的方式恢复环空完整性。本文将介绍通过连续油管下入压力激活密封胶来解决井完整性问题的操作过程。压力活化密封胶已被广泛应用于各种应用中,以有效地修复泄漏。当考虑使用密封胶修补时,首先要解决的挑战之一是如何将材料输送到泄漏部位。对于该海底油井,使用连续油管将密封胶从服务船输送到海底。然后,ROV通过飞线将线圈连接到外部采油树帽上,然后通过润滑和放压循环将密封胶引入环空。分析了环空完整性问题,以确定泄漏的严重程度和位置。在4000 psi的环空压力下,压力趋势表明泄漏范围为0.15 - 1.5 lit/min。梯度分析表明,泄漏发生在完井深处,可能在尾管接箍或封隔器处。基于这些信息,开发了一种比完井液重约2 ppg的密封胶混合物,用于封堵泄漏。在井上安装了一个外部采油树帽,以便通过热刺连接进入井的环空。大约11立方米的密封胶通过2英寸的连续油管输送到环空,该连续油管通过飞管连接到海底。为了在不超过预定压力限制的情况下实现这一目标,进行了一系列的润滑和放气循环。在密封胶沉淀在封隔器上后,保持环空压力,使密封胶在泄漏部位固化。泄漏处的压差使液体密封胶形成弹性密封。该工艺完成后不久进行了正压测试,并恢复了生产。本文将提供一个使用压力激活密封剂的例子,该密封剂设计用于仅在泄漏点聚合,为昂贵的海底油井修井提供了选择。该技术与连续油管配合使用,为解决复杂的井完整性问题提供了一种快速、经济的方法。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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