Reduced Setup Time for an SMT Line

Aurea Gama de Jesus, M. Nascimento, Paulo Francisco da Silva Ribeiro
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引用次数: 1

Abstract

The article seeks to investigate the cause in the model changeover delay in the operational process of an automatic surface mount device (SMD) insertion line of TV boards, identifying the factor that causes the time to perform SETUP using the Six Sigma to perform analysis of the results achieved. The tools applied were the process flow mapping, the Ishikawa cause and effect diagram and the Six Sigma standard planning, execution, verification and action cycle, which facilitated data collection and analysis of activities that were divided into: external and internal activities. Through this procedure it was possible to perform the recording and analysis of the data collected. The balancing of the processes and activities of the line before and during the exchange of the SETUP model, displacing external activities that were performed as internal. The next step was to standardize the activities in the process, known as Surface Mount Technology (SMT). The modification of the developed processes was of vital importance to the feeding of machines with higher quality and in a shorter time, determining and separating the common items from the exclusive ones. For this to happen, it was necessary to reprogram the machines. The model identified as critical and a 55-inch TV, the time before the study was over 80 minutes and was reduced to 40 minutes after the actions were implemented. The paper presents clearly how it was obtained and the gains in detail.
减少SMT生产线的安装时间
本文旨在研究电视板自动表面贴装装置(SMD)插入线操作过程中模型转换延迟的原因,确定导致执行SETUP时间的因素,使用六西格玛对所取得的结果进行分析。所采用的工具是过程流程图、石川因果图和六西格玛标准计划、执行、验证和行动周期,便于对活动进行数据收集和分析,活动分为:外部活动和内部活动。通过这个程序,可以对收集到的数据进行记录和分析。在SETUP模型交换之前和期间平衡流程和活动,取代作为内部执行的外部活动。下一步是标准化过程中的活动,称为表面贴装技术(SMT)。改进已开发的工艺对于在更短的时间内提供更高质量的机器,确定和分离普通物品和专用物品至关重要。为了实现这一点,有必要对机器重新编程。被认定为关键型号的55英寸电视,在研究前的时间超过80分钟,在行动实施后减少到40分钟。本文详细介绍了该方法的实现过程和所得。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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CiteScore
0.60
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0.00%
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