A. Hasanah, Tony Koerniawan, Yuliansyah Yuliansyah
{"title":"Kajian Ketelitian Current Transformer (CT) Terhadap Kesalahan Rasio Arus pada Pelanggan 197 kVA","authors":"A. Hasanah, Tony Koerniawan, Yuliansyah Yuliansyah","doi":"10.33322/ENERGI.V11I1.390","DOIUrl":null,"url":null,"abstract":"With the growth of electricity consumption getting bigger, the possibility of greater losses arises from measuring energy in customers. One cause of the losses due to mistakes in flow ratio CT (Current Transformer) installed on APP Box indirect measurement. Necessary to test the CT accuracy class to determine the current ratio error limits set by the standard PLN. Then do the replacement on the CT accuracy class to resolve this issue. This activity is done at the customer PT. Astra Int Auto 2000 by replacing the CT accuracy class of 0.5 becomes 0,5S. There is a comparison of the measurement between the two different classes. Based on the results of tests performed, a decline in the current ratio error before and after the replacement of accuracy class. After calculating the error margin of the second flow ratio CT installed that are not measured by the energy meter. This Value kWh that is the losses to PT. PLN (Persero) Area Depok. So understanding CT as one of the tools of measurement (instrumentation) should be changed to a point of transaction (point of transaction). So that the revenue gains kWh a business orientation that is fundamental to PLN by pressing slightly possible energy losses (losses) that occur in the measurement system.","PeriodicalId":377082,"journal":{"name":"Energi & Kelistrikan","volume":"137 1","pages":"0"},"PeriodicalIF":0.0000,"publicationDate":"2019-07-04","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"1","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"Energi & Kelistrikan","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.33322/ENERGI.V11I1.390","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 1
Abstract
With the growth of electricity consumption getting bigger, the possibility of greater losses arises from measuring energy in customers. One cause of the losses due to mistakes in flow ratio CT (Current Transformer) installed on APP Box indirect measurement. Necessary to test the CT accuracy class to determine the current ratio error limits set by the standard PLN. Then do the replacement on the CT accuracy class to resolve this issue. This activity is done at the customer PT. Astra Int Auto 2000 by replacing the CT accuracy class of 0.5 becomes 0,5S. There is a comparison of the measurement between the two different classes. Based on the results of tests performed, a decline in the current ratio error before and after the replacement of accuracy class. After calculating the error margin of the second flow ratio CT installed that are not measured by the energy meter. This Value kWh that is the losses to PT. PLN (Persero) Area Depok. So understanding CT as one of the tools of measurement (instrumentation) should be changed to a point of transaction (point of transaction). So that the revenue gains kWh a business orientation that is fundamental to PLN by pressing slightly possible energy losses (losses) that occur in the measurement system.
随着电力消费的增长越来越大,在客户的能量测量中可能会出现更大的损失。造成损耗的原因之一是安装在APP Box上的流量比CT(电流互感器)间接测量错误。需要对CT精度等级进行测试,以确定标准PLN设定的电流比误差限值。然后在CT精度类上进行更换,解决这个问题。该活动在客户PT. Astra Int Auto 2000上完成,将CT精度等级从0.5替换为0.5。有两个不同类别之间的测量比较。根据所进行的测试结果,电流比误差在更换精度等级之前和之后有所下降。计算出安装的第二流量比CT的误差范围后,该误差范围不是电能表测量的。该值kWh表示PT. PLN (Persero) Area Depok的损失。因此,将CT理解为测量工具(instrumentation)之一,应改为交易点(point of transaction)。因此,通过减少测量系统中可能出现的能量损失(损失),收入增加kWh,这是PLN的基本业务方向。