{"title":"Process and Energy Optimisation - A Case Study of UB FGR fan at Captive Power\nPlant of NRL","authors":"","doi":"10.33140/pcii.02.04.02","DOIUrl":null,"url":null,"abstract":"The old saying “Excellence is the gradual result of always striving to do better……. The noblest search is the\nsearch for excellence.” – An integrated approach to achieve continuous improvement and reach towards excellence\nin Utility Boiler Operation.\nThis paper highlights the case study carried out regarding the successful trial run of the Flue Gas Recirculation of\nthe Utility Boiler of Co-generation plant of the Numaligarh Refinery Limited, Golaghat, Assam. This fan could not be\nput into service since commissioning of the boiler. Once it is successfully taken into service, many positive outcomes\nare noticed and resulted in the process and energy optimization in the operation of the utility boiler.\nIn Numaligarh Refinery Limited (NRL), Co-generation plant (CGP), Utility Boiler (UB) is used to produce High\npressure super-heated steam. One of the accessories named Flue Gas Recirculation (FGR) could not be put into service\ndue to certain problems. FGR is a combustion modification process. As the name implies, a portion of the combustion\nproducts exiting the boiler are recirculated and introduced into the primary combustion zone. In UB, there are two\nnos. of FGR fans. But they could not put into service for a long time since commissioning. After a series of studies\nand experiments, the problems or factors were identified viz. Selection of correct UB load at which the fan should be\nstarted, dampers adjustment, burner flame stability, etc. After identification and trouble shooting of these problems,\nthe FGR fans could be run successfully and put into continuous service.\nFollowing advantages were achieved in UB after the service of the FGR fans\n Increases steaming rate of the U\n Saves Energy (Fuel optimization)\n Reduced harmful NOx gas Emissions\n Increased in flue gas back end temperature\n Lowers Greenhouse gas CO2\n emission as the amount of fossil fuel is reduced\nThus the above case study helped one of the important UB accessories to successfully put into service leading to\nvarious benefits, flexibility and process optimization in the operation of the UB.","PeriodicalId":355186,"journal":{"name":"Petroleum and Chemical Industry International","volume":"41 1","pages":"0"},"PeriodicalIF":0.0000,"publicationDate":"2019-09-17","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"Petroleum and Chemical Industry International","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.33140/pcii.02.04.02","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0
Abstract
The old saying “Excellence is the gradual result of always striving to do better……. The noblest search is the
search for excellence.” – An integrated approach to achieve continuous improvement and reach towards excellence
in Utility Boiler Operation.
This paper highlights the case study carried out regarding the successful trial run of the Flue Gas Recirculation of
the Utility Boiler of Co-generation plant of the Numaligarh Refinery Limited, Golaghat, Assam. This fan could not be
put into service since commissioning of the boiler. Once it is successfully taken into service, many positive outcomes
are noticed and resulted in the process and energy optimization in the operation of the utility boiler.
In Numaligarh Refinery Limited (NRL), Co-generation plant (CGP), Utility Boiler (UB) is used to produce High
pressure super-heated steam. One of the accessories named Flue Gas Recirculation (FGR) could not be put into service
due to certain problems. FGR is a combustion modification process. As the name implies, a portion of the combustion
products exiting the boiler are recirculated and introduced into the primary combustion zone. In UB, there are two
nos. of FGR fans. But they could not put into service for a long time since commissioning. After a series of studies
and experiments, the problems or factors were identified viz. Selection of correct UB load at which the fan should be
started, dampers adjustment, burner flame stability, etc. After identification and trouble shooting of these problems,
the FGR fans could be run successfully and put into continuous service.
Following advantages were achieved in UB after the service of the FGR fans
Increases steaming rate of the U
Saves Energy (Fuel optimization)
Reduced harmful NOx gas Emissions
Increased in flue gas back end temperature
Lowers Greenhouse gas CO2
emission as the amount of fossil fuel is reduced
Thus the above case study helped one of the important UB accessories to successfully put into service leading to
various benefits, flexibility and process optimization in the operation of the UB.