On the NDP onset in pre-ignition transient of high performance SRMs: VEGA Z9A experience

B. Favini, E. Cavallini, G. Rossi, M. Di Giacinto, A. Di Mascio, F. Serraglia
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引用次数: 8

Abstract

This paper discusses the early phase of the ignition transient of the VEGA Launcher's third stage solid rocket motor, Zefiro 9A. During the first two firing tests of the Z9A SRM (QM2 and VT1) a peculiar unexpected negative force peak and a significant pressure unbalance in the motor chamber were measured during the very first phase of the ignition transient. In order to fix the unexpected negative force, out of the system specifications, a modification of the igniter re-design was decided for the Z9A SRM and a third static firing test was successfully carried out (VT2), with a reduction of the negative differential pressure of at least around a factor 3, followed by a reduction of the negative thrust by around the same factor. This paper wants to analyze the scenario outlined by the VT2 static firing test by means of three dimensional unsteady multi-component numerical simulations of the SRM pre-ignition transient.
高性能srm预点火瞬态NDP开始:VEGA Z9A经验
本文讨论了VEGA发射装置第三级固体火箭发动机Zefiro 9A点火瞬变的早期阶段。在Z9A SRM (QM2和VT1)的前两次发射试验中,在点火瞬态的第一阶段测量到一个特殊的意想不到的负力峰值和电机腔内显着的压力不平衡。为了修正意外的负推力,在系统规范之外,为Z9A SRM决定了对点火器重新设计的修改,并且成功地进行了第三次静态发射试验(VT2),负压差至少减少了大约3个因素,随后负推力减少了大约相同的因素。本文通过对SRM预点火瞬态的三维非定常多分量数值模拟,对VT2静态点火试验所描绘的情景进行了分析。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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