Novel Coiled Tubing Post-Fracturing Cleanout of Unconventional Wells Without Downhole Motor: A Case Study from Argentina

Juan Martin Mirande, Giovanni Palombizio, Lucas Arevalo, Alejandro Marro, Marcelo Rodriguez, R. Krasuk, Matias Vecchietti
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Abstract

Unconventional wells that are completed with plug-and-perf fracturing techniques require coiled tubing (CT) to mill the plugs. In Argentina, CT must mill upwards of 60 plugs to bring the well into production. The CT downhole motors are leading contributors to service quality incidents because: 1) they mill challenging materials over extended periods of time, and 2) they limit the pump rate, which reduces cleanout effectiveness and increases the risk of stuck pipe. A completion campaign selected soluble plugs instead of composite ones to improve efficiency. Initial CT runs were still completed with a milling bottomhole assembly (BHA) to address the risk of low plug solubility. However, as evidenced during the initial campaign runs, the plugs dissolved nearly completely, leaving only the steel buttons inside the well. Those buttons required a high pump rate to carry them to surface. Given the excellent plug dissolution and the fluid velocity requirement to clean out buttons, the BHA was simplified to an extended reach tool (ERT) and a customized, high-rate jetting nozzle, thus eliminating the downhole motor. The new and simplified BHA extended the pump rate limit from an average of 3.8 to 4.5 bbl/min with no adverse effect on circulating pressure. The operator observed a tenfold increase in the number of plug buttons recovered at surface, which reduced the risk of stuck CT pipe during interventions in those wells. The cleanout speed was also increased, reducing total operating time by 25%, costs, and diesel consumption. A special procedure was developed for the cases when the BHA encountered consolidated sand and plug debris during the operations, a situation that occurred an average of three times per well. To clean those accumulations, the pump rate was increased to generate high jetting energy and stronger ERT agitation, and the CT was run in hole at slow speed until tagging the solids. This procedure allowed passing all the restrictions found during the execution of the CT cleanout jobs. This approach also made it possible to clean wells with known casing deformations, a common situation in Argentina unconventional wells. Over the course of 44 wells, 13 were cleaned with the simplified BHA. This new approach addressed the two main sources of nonproductive time before initiation of the project: BHA failures decreased from 16% to 8% and no CT stuck pipe event occurred. This is the first published case study of a post-fracturing cleanout in an unconventional well without the use of a downhole motor and which, instead, combined soluble plugs and a tailored BHA. Eliminating the downhole motor in this application significantly improved operational reliability and efficiency. The use of this simplified BHA to clean the well down to total depth is only possible with a good dissolution performance of the plugs present in the well.
新型连续油管压裂后无井下马达洗井技术——以阿根廷为例
采用桥塞射孔压裂技术的非常规井需要连续油管(CT)来磨铣桥塞。在阿根廷,连续油管必须磨铣60个以上的桥塞才能投产。连续油管井下马达是造成服务质量事故的主要原因,因为:1)它们需要长时间研磨具有挑战性的材料;2)它们限制了泵速,从而降低了清洗效率,增加了卡钻的风险。为了提高效率,完井作业选择了可溶性桥塞而不是复合桥塞。为了解决桥塞溶解度低的风险,连续油管的初始下入仍然使用磨铣底部钻具组合(BHA)完成。然而,在最初的作业中,桥塞几乎完全溶解,只留下钢扣留在井内。这些按钮需要很高的泵速才能将它们带到地面。考虑到出色的桥塞溶解性能和清洗按钮时对流体速度的要求,BHA被简化为一个大位移工具(ERT)和一个定制的高速喷射喷嘴,从而省去了井下马达。新型简化的底部钻具组合将泵速限制从平均3.8桶/分钟提高到4.5桶/分钟,并且对循环压力没有不利影响。作业者发现,地面回收的桥塞按钮数量增加了10倍,这降低了在修井期间连续油管卡钻的风险。清洗速度也提高了,总作业时间减少了25%,成本和柴油消耗也减少了。针对BHA在作业过程中遇到固结砂和桥塞碎屑的情况,开发了一套特殊的程序,这种情况平均每口井发生三次。为了清洁这些积垢,增加泵速以产生高喷射能量和更强的ERT搅拌,连续油管在井中以低速下入,直到标记固体。该程序允许通过在连续油管清洗作业执行过程中发现的所有限制。这种方法还可以清洗已知套管变形的井,这在阿根廷非常规井中很常见。在44口井的作业过程中,使用简化的BHA对13口井进行了清洗。这种新方法解决了项目开始前非生产时间的两个主要来源:BHA失效从16%下降到8%,没有发生连续油管卡钻事件。这是首次在没有使用井下马达的情况下,在非常规井中进行压裂后清洗的案例研究,而是将可溶性桥塞和定制的BHA结合在一起。在这种应用中,取消井下马达可以显著提高作业的可靠性和效率。使用这种简化的BHA清洁井至总深度,只有在良好溶解井中桥塞的情况下才有可能。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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