Recover Stuck Drill Pipe in an Uncontrolled Well with Abrasive Cutting Technique on Coiled Tubing – Case Study

Nestor Mesa, Camilo Perez, Eddisson Aldana, Carolina Sanchez, Oswaldo Silva
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Abstract

Drilling low-pressure formations represent challenges. In the present paper, an operational situation became an issue when during the drilling of a deviated well, the circulation was lost, and the BHA got stuck, followed by a gas inflow observed in the return line. After a well control procedure and several failed attempts to control the well and recover the drilling BHA, another problem occurred when the drill pipe got plugged, making it impossible to continue pumping control pills. The scenario described above was presented to the Coiled Tubing and Thru Tubing companies with the request of a proposal to help solve three specific goals to achieve remove the plug in the inner of the drill pipe, getting communication between the drill pipe and the open hole to be able to pump Lost Control Material (LCM) and control de well, perform a cut of the drill pipe in case the pipe couldn't be recover after control the gas inflow. With an interdisciplinary group, the problem was analyzed, and a proposal was submitted, including three runs with Coiled Tubing and Thru Tubing tools. The first run a cleanout of the drill pipe with a downhole motor and taper mill. The second run will be with an abrasive punching BHA to establish communication with the annuls, and the third run will be for an abrasive cutting that will allow the recovery of the drill pipe above the free point. The job preparation includes the engineering program with the operational parameters and flow chart and the logistic preparation with the resources such as coiled tubing equipment, thru-tubing BHAs, chemicals, and fluids, among others. During the operation, other discussions and revisions forced a change in the plan from the initial proposal, performing two of the three runs for the cleanout and abrasive cutting, which represented a benefit by controlling the well with the slurry pumped working as a LCM that helped control the gas inflow. With a conclusion of a successful cut and drill pipe recovery, the operation data and analysis of the preparation vs. the execution are presented in the paper.
连续油管磨料切削技术在非受控井中回收卡钻-实例分析
钻探低压地层是一个挑战。在本文中,在斜井的钻井过程中,出现了一种作业情况,即循环丢失,底部钻具组合卡住,然后在回油管中观察到气体流入。在进行了一次井控程序,并多次尝试控制井和恢复钻井BHA失败后,钻杆被堵塞,导致无法继续泵送控制丸,这又出现了另一个问题。上述场景被提交给连续油管和直通油管公司,要求解决三个具体目标:移除钻杆内部的塞,在钻杆和裸眼之间建立通信,以便能够泵送失控物质(LCM)并控制井,在控制气体流入后无法恢复钻杆的情况下切割钻杆。与跨学科小组一起,对问题进行了分析,并提交了一份方案,其中包括使用连续油管和直通油管工具的三次下入。第一次下入使用井下马达和锥形铣刀对钻杆进行清洗。第二次下入将使用磨料冲孔BHA与环空建立联系,第三次下入将使用磨料切割,使钻杆在空闲点以上恢复。作业准备包括工程方案、作业参数和流程图,以及物流准备,包括连续油管设备、直通油管bha、化学品和流体等资源。在作业过程中,其他讨论和修订迫使计划从最初的建议进行了改变,进行了三次入井中的两次清洗和磨料切割,这代表了通过泵送泥浆作为LCM来控制井的好处,有助于控制气体流入。本文总结了一次成功的岩屑和钻杆回收,给出了作业数据,并对准备和执行进行了分析。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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