Case Study: Rejuvenation Fluid Injection Results from Duke Power's Little Rock Retail Tap Line

W. Stagi, F.E. Kimsey
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引用次数: 1

Abstract

In 1994, a Duke Power Company, 115 kV class, XLPE underground transmission cable failed. Failure analysis performed by Cable Technology Laboratories noted a low ac breakdown strength and suggested a high insulation moisture content as a likely reason. Duke Power opted to treat the remaining (un-failed) cables using CableCUREreg life-extension, fluid injection technology. The treated cables remained in service for an additional 10 years after injection. Ultimately a termination failure led to the decision to remove them from service. This allowed an unprecedented opportunity to evaluate the responsiveness of solid dielectric, transmission cables to fluid treatment. Until now most of the 60,000,000 feet of injected cable has been in the distribution class of cables. The results of that evaluation, published in this paper, demonstrate treatment effectiveness on par with results obtained on distribution class cables
案例研究:来自杜克电力公司小石城零售自来水管线的回春液注射结果
1994年,杜克电力公司的一条115千伏级、XLPE地下输电电缆发生故障。电缆技术实验室进行的故障分析指出,交流击穿强度低,并建议高绝缘含水率可能是原因。杜克电力公司选择使用CableCUREreg延长使用寿命的流体注入技术来处理剩余的(未损坏的)电缆。经过处理的电缆在注入后可继续使用10年。最终,终止失败导致决定将其从服务中移除。这为评估固体介质、传输电缆对流体处理的响应性提供了前所未有的机会。到目前为止,6000万英尺注入电缆中的大部分都是配电电缆。该评估结果发表在论文中,证明了处理效果与配电级电缆的结果相当
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