Effect of transformer connection and construction on single phasing detection

G. Johnson, R. Hamilton, S. Thakur
{"title":"Effect of transformer connection and construction on single phasing detection","authors":"G. Johnson, R. Hamilton, S. Thakur","doi":"10.1109/CPRE.2013.6822036","DOIUrl":null,"url":null,"abstract":"On January 30, 2012, Unit 2 at Exelon Corporation's Byron Generating Station experienced an event that resulted in a unit trip and a loss of offsite power to the unit. The root cause of the event was determined to be the failure of an under hung insulator on the phase C feed to the Unit 2 Station Auxiliary Transformers (SAT). An insulator on a bus support broke and grounded the high voltage bushing of the SAT, causing a short section of 345 kV bus to become disconnected. The section on the SAT side also fell to ground. See Figure 1. This bus section was associated with the phase C offsite source to the SATs. This event caused an open circuit on phase C; however, neither the protective relay system in the switchyard nor the plant relaying detected the loss of phase C. This paper will provide an outline of the event, failure analysis and follow-up actions as a result of the event, including a microprocessor based relay solution, as well as transformer theory relevant to single phasing issue.","PeriodicalId":221348,"journal":{"name":"2013 66th Annual Conference for Protective Relay Engineers","volume":"13 1","pages":"0"},"PeriodicalIF":0.0000,"publicationDate":"2013-04-08","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"2","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"2013 66th Annual Conference for Protective Relay Engineers","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.1109/CPRE.2013.6822036","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 2

Abstract

On January 30, 2012, Unit 2 at Exelon Corporation's Byron Generating Station experienced an event that resulted in a unit trip and a loss of offsite power to the unit. The root cause of the event was determined to be the failure of an under hung insulator on the phase C feed to the Unit 2 Station Auxiliary Transformers (SAT). An insulator on a bus support broke and grounded the high voltage bushing of the SAT, causing a short section of 345 kV bus to become disconnected. The section on the SAT side also fell to ground. See Figure 1. This bus section was associated with the phase C offsite source to the SATs. This event caused an open circuit on phase C; however, neither the protective relay system in the switchyard nor the plant relaying detected the loss of phase C. This paper will provide an outline of the event, failure analysis and follow-up actions as a result of the event, including a microprocessor based relay solution, as well as transformer theory relevant to single phasing issue.
变压器接线及施工对单相检测的影响
2012年1月30日,Exelon公司拜伦电站2号机组发生事故,导致机组发生故障,机组失去了场外供电。事件的根本原因被确定为2号机组辅助变压器(SAT)的C相馈电的下挂绝缘子失效。母线支架上的绝缘子断开并接地了SAT的高压套管,导致345千伏母线的一小段断开。SAT一侧的部分也掉到了地上。参见图1。该总线部分与阶段C的场外源连接到sat。该事件导致C相断路;然而,开关站中的保护继电器系统和工厂继电器都没有检测到c相的丢失。本文将提供事件的概述,故障分析和后续行动,包括基于微处理器的继电器解决方案,以及与单相问题相关的变压器理论。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
求助全文
约1分钟内获得全文 求助全文
来源期刊
自引率
0.00%
发文量
0
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
确定
请完成安全验证×
copy
已复制链接
快去分享给好友吧!
我知道了
右上角分享
点击右上角分享
0
联系我们:info@booksci.cn Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。 Copyright © 2023 布克学术 All rights reserved.
京ICP备2023020795号-1
ghs 京公网安备 11010802042870号
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术官方微信