History of Managing Productivity Issues Due to Fines Migration in a Malaysian Oil Field Offshore Sarawak

Amir Irfan Mahra, Ryan Guillory, R. Islamov, Gurveen Singh Reekhi Satwant, Nurul Asyikin Mohd Radzuan, F. A. Salleh, Tunku Indra Tunku Abdul Muthalib
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Abstract

Field D (offshore Sarawak, Malaysia) first production was in 2012 from three wells, with a second phase of development in 2017 with the drilling of four wells. Severe productivity decline was seen in five of the seven wells, and numerous studies were completed to narrow in on the root causes. Several production enhancement techniques were executed on Phase 1 and Phase 2 wells, where learnings and results will be further shared. Prior to the drilling of six additional wells in Phase 3 (2020), additional detailed lab studies were undertaken, and new strategies were implemeted based on this were applied with encouraging results. The majority of the wells have downhole pressure gauges (PDG), and coupled with frequent well test data, PTA, and Nodal Analysis modeling Productivity Index, permeability thickness (kH), and Skin are able to be tracked over time. By trending these different productivity indicators, it became clear that formation damage was occurring in several wells with varying degrees of severity based on the performance of the reservoir layer being produced. Various formation damage mechanisms were assessed (scale, wax, asphaltenes, drilling & completion damage, fines migration), and based on the initial study it was determined that fines migration was likely the major issue. Historically, no sand was observed on the surface where monthly sand count reported has always been <1 pound per thousand bbl (pptb) which was supported by geomechanics, and sand failure tendency studies completed during development phase of the field. Hence, six of the seven Phase 1 and 2 wells were completed with cased and perforated strategy with no downhole sand control, with the other well completed as a highly deviated open hole standalone completion. The productivity declines were only experienced in the cased and perforated completions, which had much lower gross completed interval and thus experienced higher velocities near the wellbore. The main production enhancement strategy applied to date has been re-perforation (8 re-perforation jobs), with varying degrees of productivity improvement and duration of sustainability. Solid propellant technology was applied in one of the well and clearing of the perforation tunnels via through-tubing dynamic underbalance technique in two wells was applied and no major improvement in sustained production impact was observed. An acid stimulation was recently pumped for the first time in one well and the assessment details will be shared, and results of the pumping will be shared in detail. At the time of the paper, no post production results were available. Prior to the drilling of six Phase 3 wells in 2020, detailed lab studies to look at the impact of various drilling muds were assessed, and learnings were incorporated in the mud program. Critical velocity studies were completed, and learnings from this work such as well ramp-up strategy and normalized maximum production rates have been added to the well-by-well production strategy. Based on Phase 3 production data to date, application of these new learnings has resulted in no major productivity decline seen. The learnings from D field would benefit other operators by sharing the lessons learned on assessment of formation damage mechanisms, the results of the different type of production enhancements applied, and the successful mitigation strategies for future wells (lab assessment, mud strategy change, and production strategies to prevent plugging due to fines migration).
马来西亚沙捞越近海油田罚款迁移导致生产力问题的管理历史
油田D(马来西亚Sarawak海上)于2012年首次生产3口井,2017年进行了第二阶段的开发,钻了4口井。7口井中有5口出现了严重的产能下降,为了缩小根本原因,研究人员进行了大量研究。在1期和2期井中实施了几种增产技术,这些技术的学习和成果将进一步分享。在第三阶段(2020年)再钻6口井之前,进行了更多详细的实验室研究,并在此基础上实施了新的策略,取得了令人鼓舞的结果。大多数井都有井下压力表(PDG),再加上频繁的试井数据、PTA和节点分析模型,可以随时间跟踪产能指数、渗透率厚度(kH)和表皮。通过对这些不同产能指标的趋势分析,可以清楚地看到,根据所产储层的表现,几口井的地层损害程度各不相同。评估了各种地层损害机制(结垢、结蜡、沥青质、钻完井损害、细颗粒运移),根据初步研究,确定细颗粒运移可能是主要问题。从历史上看,地面没有观察到砂,每月报告的出砂量一直小于1磅/千桶(pptb),这得到了地质力学的支持,并且在油田开发阶段完成了出砂趋势研究。因此,7口第一期和第二期井中有6口采用套管射孔方法完成,没有井下防砂,另一口井采用大斜度裸眼独立完井。产能下降只发生在套管井和射孔完井中,这些完井的总完井段要小得多,因此井筒附近的速度更高。迄今为止应用的主要增产策略是再射孔(8次再射孔作业),以不同程度的提高生产率和持续时间。其中一口井采用固体推进剂技术,两口井采用过油管动态欠平衡技术清理射孔孔道,对持续生产影响没有明显改善。最近在一口井中首次进行了酸增产作业,评估细节将被分享,泵注结果将被详细分享。在撰写本文时,尚无后期制作结果。在2020年钻探6口三期井之前,对各种钻井泥浆的影响进行了详细的实验室研究,并将研究成果纳入了泥浆项目。临界速度研究已经完成,从这项工作中获得的经验教训,如井的增产策略和标准化的最大产量,已经被添加到逐井的生产策略中。根据迄今为止第三阶段的生产数据,这些新知识的应用并没有导致重大的生产力下降。D油田的经验教训将使其他作业者受益,分享有关地层损害机制评估的经验教训,不同类型增产措施的应用结果,以及未来油井的成功缓解策略(实验室评估、泥浆策略的改变,以及防止细颗粒运移造成堵塞的生产策略)。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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