Recent Experience in Squeeze Treating Huff and Puff Wells for Control of Steamflood Generated Calcium Carbonate Scale

A. Thornton, Yaz Belhimer, I. Smith, A. Subramaniyan
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Abstract

Steamflooding technology introduction into hydrocarbon recovery operations often brings with it unwanted unavoidable mineral scaling challenges. In this example, steamflood generated calcium carbonate scale caused downhole equipment failure during cyclical steamflood stimulation (CSS) operations. The precipitated scale was effectively removed via mineral acid tubing wash, however mineral acid use for ad-hoc scale dissolving duty added significantly to the corrosion burden of well production tubing strings already regularly exposed to aggressive high concentration mineral acid during near wellbore matrix stimulation treatments. Scale inhibitor squeezing was proposed as a proactive alternative to mineral acid for downhole scale mitigation, and is the subject of this case history. The Middle Eastern heavy oil (HO) field has experience in employing scale inhibitors for topside scale control, but has limited experience in scale squeezing, and no experience of scale squeezing cyclical steam flooded wells. The initiative therefore presented some interesting challenges with respect to the Scale inhibitor selection (thermal stability concerns, compatibility and calcium carbonate efficacy concerns), where to place the scale squeeze in the CSS treatment programme, the squeeze design and its placement within the CSS well, and introduction and execution of routine well scaling health monitors for assessing the performance of the scale squeeze across the full CSS life-cycle. Detailed bullheaded scale squeeze designs were prepared for two pilot HO field CSS wells that had experienced CaCO3 scaling. Once prepared, the squeeze treatments were quickly scheduled and executed without significant issue - either during treatment application or post-squeeze/steamflood return. The well brine monitors (brine ion composition, residual scale inhibitor and suspended solids) revealed interesting trends during the surveillance phase, but most importantly showed that the scale squeezes performed according to design and successfully maintained the wells free of CaCO3 scale, up to and including the 266 days post-steamflood, at which point routine well produced water sampling was discontinued. After 360 days (at the final review meeting) the field operators advised that both squeezed wells were still in operation and had experienced no scaling downtime.
挤压处理吞吐井控制蒸汽驱碳酸钙结垢的新经验
将蒸汽驱技术引入油气开采作业中,往往会带来不可避免的矿物结垢问题。在本例中,在循环蒸汽驱增产(CSS)作业中,蒸汽驱产生的碳酸钙结垢导致井下设备故障。通过矿酸洗油管可以有效地去除沉淀的水垢,然而,在近井基质增产处理过程中,用于特殊溶解水垢的矿酸大大增加了油井生产管柱的腐蚀负担,这些管柱已经经常暴露在高浓度矿酸中。缓蚀剂挤压被认为是一种主动替代矿物酸的井下阻垢剂,也是本案例的主题。中东稠油(HO)油田有使用阻垢剂控制上层结垢的经验,但在压垢方面的经验有限,更没有循环蒸汽驱井压垢的经验。因此,该计划提出了一些有趣的挑战,包括阻垢剂的选择(热稳定性问题、兼容性问题和碳酸钙有效性问题)、在CSS处理方案中放置阻垢剂的位置、阻垢剂的设计及其在CSS井中的位置,以及常规井结垢健康监测的引入和执行,以评估阻垢剂在整个CSS生命周期中的性能。对两口经历CaCO3结垢的试验井进行了详细的井口压垢设计。一旦准备好,无论是在处理过程中还是在挤压/蒸汽驱后,都可以快速安排和执行挤压处理,没有出现重大问题。在监测阶段,油井卤水监测(卤水离子组成、残留阻垢剂和悬浮固体)揭示了有趣的趋势,但最重要的是,根据设计进行的结垢挤压成功地保持了油井无CaCO3结垢,直至蒸汽驱后的266天,此时常规的采出水采样停止。360天后(在最后的审查会议上),现场作业人员建议,这两口被挤压的井仍在运行,没有发生结垢停机。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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