Application of gas-assisted gravity drainage (GAGD) to improve oil recovery of Rang Dong basement reservoir

K. Nguyen, Minh Dung Ha
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Abstract

As an option to improve the ultimate oil recovery factor of the Rang Dong field, a feasibility study of gas-assisted gravity drainage (GAGD) application was carried out for the fractured basement reservoir with a single-well Huff ‘n’ Puff pilot test applied on a high water-cut producer. This paper aims to provide an in-depth understanding about such case study, which includes details on candidate selection, gas injection scheme, on-site execution, results of flow-back, post-job review and lessons learned. The pilot test of GAGD was recorded with a good oil rate and low water-cut during flowing back after gas injection and shut-in for gas segregation, which suggests the positive effectiveness of GAGD to some degree. The expansion of the GAGD application to other wells and areas in the field would be encouraged in any similar situation. On the other hand, the results of this pilot test shed a light into further optimisation of the candidate selection and gas injection scheme by material balance analysis and reservoir simulation respectively.
气辅重力抽采在让东基底油藏提高采收率中的应用
为了提高Rang Dong油田的最终采收率,对裂缝性基底油藏进行了气体辅助重力驱油(GAGD)的可行性研究,并在高含水油藏上进行了单井Huff ' n ' Puff先导试验。本文旨在深入了解此类案例研究,包括候选人选择,注气方案,现场执行,返排结果,作业后回顾和经验教训等细节。GAGD中试结果表明,在注气、关井分离后的回排过程中,GAGD的产油速率好,含水率低,具有一定的积极效果。在任何类似的情况下,将鼓励将GAGD应用扩展到现场的其他井和区域。另一方面,该先导试验的结果分别为通过物质平衡分析和储层模拟进一步优化候选层选择和注气方案提供了线索。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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