某炼油厂原油蒸馏装置侧切管中汽油泄漏

IF 4.8 Q2 ENERGY & FUELS
Chidambaram Subramanian
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引用次数: 7

摘要

本文报道炼油厂燃气管道使用三年后侧切弯管失效,管道材质为SS316L奥氏体不锈钢。系统的调查包括目视检查和实验室研究,以确定故障的原因。对失效部位的试样进行了化学分析、硬度、断口分析、元素分析和金相评价。此外,还对原料进行了评价。各种表征研究得出结论,在初始精馏塔(侧切管道)操作开始之前,存在密封在弯头中的材料缺陷是故障的根本原因。内压引起的局部应力作用于剩余壁厚,导致脆性断裂,导致油气泄漏。失效弯头在初次运行前存在材料缺陷,表明调试前检查工作不到位。讨论了检测到的材料缺陷的来源,并且在关键管道位置提供适当的支撑系统的无缺陷管道部件应避免类似的泄漏。本文的结果适用于炼油厂管道/能源管道操作员,用于在关键位置使用合格的管道组件,特别是在工厂/管道调试阶段。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Leakage of gasoil from side cut piping in crude distillation unit of a petroleum refinery

This paper reports failure of elbow from side cut piping after three years of refinery gasoil service and piping metallurgy was SS316L austenitic stainless steel. Systematic investigations including visual inspection coupled with laboratory studies were carried out to determine the cause of failure. The samples from failure location were examined for chemical analysis, hardness, fractography, elemental analysis and metallographic evaluation. Further, crude feedstock was evaluated as well. Various characterization studies concluded that presence of material defect encapsulated in elbow prior to start of initial distillation column (side cut piping) operation was the root cause of failure. Localized stresses induced from internal pressure act on remaining wall thickness have lead to brittle fracture and resulted in gasoil leakage. The existence of material defect in failed elbow prior to initial operation had revealed poor pre-commissioning inspection practice. The origination of detected material defect was discussed and similar leakages shall be avoided by defect free piping components provided with proper support system at critical piping locations. The results in this article intended for petroleum refinery piping/energy pipeline operators for use of qualified piping components at critical locations especially during plant/piping commissioning stage.

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CiteScore
7.50
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