A. Shakhova, Natalia Lisyutina, I. Lebedeva, Oleg Valshin, Roman Savinov, Robert Famiev, A. Dementyev, D. Marushkin, V. Bochkarev, Vladimir Surmin, E. Bolychev
{"title":"Odoptu-More油田利用多边钻井技术进行ERD井的远程油藏勘探","authors":"A. Shakhova, Natalia Lisyutina, I. Lebedeva, Oleg Valshin, Roman Savinov, Robert Famiev, A. Dementyev, D. Marushkin, V. Bochkarev, Vladimir Surmin, E. Bolychev","doi":"10.2118/206450-ms","DOIUrl":null,"url":null,"abstract":"\n This paper provides the results that were achieved and shares the drilling unique practices that were implemented to deliver the first complex bilateral extended reach drilling (ERD) well in Odoptu-more field (North Dome).\n Well design driven by geological objectives considered drilling 215.9mm main and pilot holes (PH). Well complexity was governed by the type of a profile having ERD ratio of 5.22 (main hole) / 4.60 (PH) and trajectory's 3D nature (turn in azimuth of 90 degrees) compared to previous wells in the project drilled mainly with 2D profiles. Apart from the problems connected with drilling and casing upper sections key challenges comprised kicking off in 215.9mm open hole at 5955m MD and 1512m TVD with rotary steerable system, setting cement plugs at shallow true vertical depth (TVD) at 89 degrees of inclination to abandon laterally drilled PH, delivering 168.3mm production liner to bottom with a risk of entering a lateral while running in hole.\n An effective collaboration between integrated engineering team and customer departments went far beyond ERD standard set of operations already existing in the project thus allowing to break its own records and to set new achievements due to integrated technological approach. The longest 444.5mm section (2975 m) was drilled in one run achieving the record daily drilling rate and rate of penetration (ROP). Cementing of 244.5mm floated liner resulted in the highest good cement bond integrity percentage ever achieved among other wells in project due to new ways of casing standoff and fluid rheology hierarchy modeling. For the first time in the project 215.9mm main horizontal hole in extreme reach ERD well has been drilled by kicking off in open hole from the pilot horizontal one with push-the-bit rotary steerable system without a kickoff plug with pilot hole being abandoned by setting cement plugs. Project-specific risk assessment conducted by team allowed successful deployment of 168.3mm liner into the main hole. Moreover, due to thorough engineering planning electrical submersible pump (ESP) was run without extending 244.5mm liner to surface by tie-back thus saving additional 7 days.\n Drilling first bilateral ERD well unlocked opportunities for the operator to reach, explore and develop different extended geological targets thus eliminating well construction process of additional wells on drilling upper sections.","PeriodicalId":11017,"journal":{"name":"Day 2 Wed, October 13, 2021","volume":"27 1","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2021-10-12","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":"{\"title\":\"Remote Reservoir Exploration in Odoptu-More Field by Delivering ERD Wells Using Multilateral Drilling Technology\",\"authors\":\"A. Shakhova, Natalia Lisyutina, I. Lebedeva, Oleg Valshin, Roman Savinov, Robert Famiev, A. Dementyev, D. Marushkin, V. Bochkarev, Vladimir Surmin, E. Bolychev\",\"doi\":\"10.2118/206450-ms\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"\\n This paper provides the results that were achieved and shares the drilling unique practices that were implemented to deliver the first complex bilateral extended reach drilling (ERD) well in Odoptu-more field (North Dome).\\n Well design driven by geological objectives considered drilling 215.9mm main and pilot holes (PH). Well complexity was governed by the type of a profile having ERD ratio of 5.22 (main hole) / 4.60 (PH) and trajectory's 3D nature (turn in azimuth of 90 degrees) compared to previous wells in the project drilled mainly with 2D profiles. Apart from the problems connected with drilling and casing upper sections key challenges comprised kicking off in 215.9mm open hole at 5955m MD and 1512m TVD with rotary steerable system, setting cement plugs at shallow true vertical depth (TVD) at 89 degrees of inclination to abandon laterally drilled PH, delivering 168.3mm production liner to bottom with a risk of entering a lateral while running in hole.\\n An effective collaboration between integrated engineering team and customer departments went far beyond ERD standard set of operations already existing in the project thus allowing to break its own records and to set new achievements due to integrated technological approach. The longest 444.5mm section (2975 m) was drilled in one run achieving the record daily drilling rate and rate of penetration (ROP). Cementing of 244.5mm floated liner resulted in the highest good cement bond integrity percentage ever achieved among other wells in project due to new ways of casing standoff and fluid rheology hierarchy modeling. For the first time in the project 215.9mm main horizontal hole in extreme reach ERD well has been drilled by kicking off in open hole from the pilot horizontal one with push-the-bit rotary steerable system without a kickoff plug with pilot hole being abandoned by setting cement plugs. Project-specific risk assessment conducted by team allowed successful deployment of 168.3mm liner into the main hole. 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Remote Reservoir Exploration in Odoptu-More Field by Delivering ERD Wells Using Multilateral Drilling Technology
This paper provides the results that were achieved and shares the drilling unique practices that were implemented to deliver the first complex bilateral extended reach drilling (ERD) well in Odoptu-more field (North Dome).
Well design driven by geological objectives considered drilling 215.9mm main and pilot holes (PH). Well complexity was governed by the type of a profile having ERD ratio of 5.22 (main hole) / 4.60 (PH) and trajectory's 3D nature (turn in azimuth of 90 degrees) compared to previous wells in the project drilled mainly with 2D profiles. Apart from the problems connected with drilling and casing upper sections key challenges comprised kicking off in 215.9mm open hole at 5955m MD and 1512m TVD with rotary steerable system, setting cement plugs at shallow true vertical depth (TVD) at 89 degrees of inclination to abandon laterally drilled PH, delivering 168.3mm production liner to bottom with a risk of entering a lateral while running in hole.
An effective collaboration between integrated engineering team and customer departments went far beyond ERD standard set of operations already existing in the project thus allowing to break its own records and to set new achievements due to integrated technological approach. The longest 444.5mm section (2975 m) was drilled in one run achieving the record daily drilling rate and rate of penetration (ROP). Cementing of 244.5mm floated liner resulted in the highest good cement bond integrity percentage ever achieved among other wells in project due to new ways of casing standoff and fluid rheology hierarchy modeling. For the first time in the project 215.9mm main horizontal hole in extreme reach ERD well has been drilled by kicking off in open hole from the pilot horizontal one with push-the-bit rotary steerable system without a kickoff plug with pilot hole being abandoned by setting cement plugs. Project-specific risk assessment conducted by team allowed successful deployment of 168.3mm liner into the main hole. Moreover, due to thorough engineering planning electrical submersible pump (ESP) was run without extending 244.5mm liner to surface by tie-back thus saving additional 7 days.
Drilling first bilateral ERD well unlocked opportunities for the operator to reach, explore and develop different extended geological targets thus eliminating well construction process of additional wells on drilling upper sections.