蒸汽出口收集器出现故障

T. D. da Silveira, I. Le May
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引用次数: 0

摘要

发电机中的过热器在400℃和41 kPa下产生80 t/h的蒸汽。故障发生在从收集器到启动期间使用的排气管道的连接处。结构材料为碳钢,故障时机组运行24万小时,停机99次。内部明显出现了广泛的裂缝,最严重的裂缝出现在离喷嘴连接处一段距离处的下游方向。安全阀和吹灰器连接处也出现了广泛的开裂和麻点。在壳孔的下游,点蚀最为明显。在所有的破坏区域,破坏机制涉及表面点蚀和随后的SCC。这一故障表明,在可能发生冷凝并定期返回过热器或其他热部件的长管路中可能出现的问题。在这种特殊情况下,对锅炉给水中溶解固体的控制可能是不够的。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Failure at a Steam Outlet Collector
A superheater in a generator produced 80 t/h of steam at 400 deg C and 41 kPa. Failure took place at the connection from the collector to the vent line used during start up. The material of construction was carbon steel, and the unit had 240,000 h of operation at the time of failure, with 99 shutdowns. Widespread cracking on the inside was apparent, the most severe cracking being some distance from the nozzle connection in a downstream direction. Widespread cracking and pitting were observed also at the connections to the safety valve and soot blower. Pitting was most apparent on the downstream sides of the openings in the shell. In all the damaged areas the mechanism of failure involved surface pitting and subsequent SCC. This failure showed the problems that can develop where there are long lines in which condensation may occur and return periodically to a superheater or other hot component. In this particular case, control of dissolved solids in the boiler feedwater may have been inadequate.
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