敏化阀杆的应力腐蚀开裂失效

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引用次数: 0

摘要

用于操作蒸汽发电厂闸阀的17-4 PH (AISI 630型)不锈钢阀杆,在暴露于175摄氏度(350华氏度)和11兆帕(1600 psi)的高纯净水中大约四个月后失效。据报道,阀杆在1040 +/-14摄氏度(1900 +/-25华氏度)下进行了30分钟的固溶热处理,空气淬火或油淬火至室温。然后据报道,茎在550到595摄氏度(1025到1100华氏度)下老化4小时。调查(目视检查,0.7x/50x图像,硬度测试,再热处理和金相检查)支持了失效是由应力集中引起的渐进SCC引起的结论。此外,固溶热处理或被省略或在过高的温度下进行,而时效处理在过低的温度下进行。建议包括以下热处理方法:锻造后,在1040℃(1900°F)下固溶热处理1小时,然后油淬火;为了避免对SCC的易感,在595摄氏度(1100华氏度)下放置4小时,然后风冷。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Stress-Corrosion Cracking Failure of a Sensitized Valve Stem
A valve stem made of 17-4 PH (AISI type 630) stainless steel, which was used for operating a gate valve in a steam power plant, failed after approximately four months of service, during which it had been exposed to high-purity water at approximately 175 deg C (350 deg F) and 11 MPa (1600 psi). The valve stem was reported to have been solution heat treated at 1040 +/-14 deg C (1900 +/-25 deg F) for 30 min and either air quenched or oil quenched to room temperature. The stem was then reportedly aged at 550 to 595 deg C (1025 to 1100 deg F) for four hours. Investigation (visual inspection, 0.7x/50x images, hardness testing, reheat treatment, and metallographic examination) supported the conclusion that failure was by progressive SCC that originated at a stress concentration. Also, the solution heat treatment had been either omitted or performed at too high of a temperature, and the aging treatment had been at too low of a temperature. Recommendations included the following heat treatments: after forging, solution heat treat at 1040 deg C (1900 deg F) for one hour, then oil quench; to avoid susceptibility to SCC, age at 595 deg C (1100 deg F) for four hours, then air cool.
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