Fracture of a Cast Stainless Steel Lever Because of a Cold Shut

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Abstract

A lever (machined from a casting made of AISI type 410 stainless steel, then surface hardened by nitriding) that was a component of the main fuel-control linkage of an aircraft engine fractured in flight after a service life of less than 50 h. Investigation (radiographic inspection) supported the conclusions that the lever broke at a cold shut extending through approximately 95% of the cross section. The normally applied load constituted an overload of the remainder of the lever. Recommendations included adding magnetic-particle inspection to the inspection procedures for this cast lever.
铸造不锈钢拉杆因冷关闭而断裂
飞机发动机主要燃油控制连杆部件的杠杆(由AISI 410型不锈钢铸件加工,然后通过氮化表面硬化)在飞行中断裂,使用寿命不到50小时。调查(射线检查)支持的结论是,杠杆在冷关闭时断裂,延伸到大约95%的横截面。正常施加的载荷构成了杠杆剩余部分的过载。建议包括在这个铸造杠杆的检查程序中增加磁粉检查。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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