Reducing the Defects of A-Pillar Stamping Part in the Automotive Assembly Process

Hassakorn Rojpitinithikorn, Jing Tang, N. Leelawat
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Abstract

This research aims to reduce defect in the automotive assembly process. Considering the defect and cost that occurred during one year; the highest defect cost came from the A-Pillar stamping part. Therefore, we analyzed production process as well as finding out the cause of the problems that occur in the stamping process by using Failure Mode and Effect Analysis (FMEA) to analyze it and conduct experiments by Design of Experiment (DOE) method. The results found that the problem came from the design of metal stamping die are not good enough to produce large parts, which are the risk of spring back problems of parts. After improving the stamping process by adding re-strike die; it is expected to reduce the number of defect from 492 cases to be zero and save the defect cost amount of 27 million Thai Baht per year.
减少汽车装配过程中a柱冲压件的缺陷
本研究旨在减少汽车装配过程中的缺陷。考虑一年内发生的缺陷和成本;缺陷成本最高的是a柱冲压件。因此,我们对生产过程进行了分析,并通过失效模式和影响分析(FMEA)对冲压过程中出现的问题进行了分析,并通过实验设计(DOE)方法进行了实验。结果发现,问题来源于金属冲压模具的设计不够好,不能生产大型零件,这是零件回弹问题的风险。改进冲压工艺后,加入重冲模;预计将使缺陷数量从492件减少到零,每年可节省2700万泰铢的缺陷费用。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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