Failure of Steam Pipe at Local Defects

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Abstract

During a hydraulic test on one of the boilers in a range, leakage occurred from the lower surface of a horizontal S bend in the main steam pipe between the drum connector box and the junction valve. The pipe in question was 15 in. bore and had been in service for about 50 years. Specimens were prepared for microscopical examination to include the defective zone and a section through a circumferential crack. The defective zone was found to contain numerous inclusions of slag and oxides of globular form. Regions surrounding the inclusions were decarburized, the indications being that this region of the plate had been heated to an excessively high temperature. A corrosion-fatigue fissure was at one location, this having originated at the internal surface of the pipe and run into an inclusion in the defective zone. The failure resulted from the development of corrosion-fatigue fissures which originated at a zone containing defects introduced at the time of manufacture. These may have had their origin in the ingot from which the plate was rolled or, alternatively, be indicative of a zone which suffered overheating and local burning at the time the forge weld was made.
蒸汽管道在局部缺陷处失效
在某锅炉的水力试验中,泄漏发生在汽包连接盒和连接阀之间的主蒸汽管道水平S型弯道的下表面。有问题的管子是15英寸。钻孔和已经使用了大约50年。准备标本进行显微镜检查,包括缺陷区和通过圆周裂纹的截面。发现缺陷区含有大量球状的渣和氧化物夹杂物。夹杂物周围的区域脱碳,表明这片区域被加热到过高的温度。腐蚀疲劳裂纹出现在一个位置,该裂纹起源于管道的内表面,并在缺陷区遇到夹杂物。破坏是由于在制造时引入的含有缺陷的区域产生了腐蚀疲劳裂纹。这些缺陷可能源于轧制钢板的铸锭,或者,也可能表明在锻造焊接时某个区域遭受过热和局部燃烧。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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