Failure of Propeller Attachment Bolts

C. Craft
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Abstract

The propeller from a small private airplane came off in flight. The head ends of all six attachment bolts remained in the propeller hub when it was found. Two threaded shanks with nuts remained with the engine, while the remaining four shank ends with their nuts were missing. Parts available for examination, in addition to the hub and attachment bolts, were the two propeller blades and the engine crankshaft. The purpose of this examination was to determine the nature and probable cause of failure in the six attachment bolts. Indications of fatigue failure and wear were the major findings in visual and low power microscopic examination. Fracture surfaces indicated failure was initiated in the threads in four bolts and in the shanks in two. The group of four bolts failed primarily due to tensile loads, while the other two bolts failed primarily due to bending loads. It was concluded that failure was due to improper installation torqueing of the bolts.
螺旋桨连接螺栓失效
一架小型私人飞机的螺旋桨在飞行中脱落了。当它被发现时,所有六个附件螺栓的头端仍然在螺旋桨轮毂。两个带螺母的螺纹柄留在发动机上,而剩下的四个带螺母的柄端不见了。除了轮毂和附属螺栓外,可供检查的部件还有两个螺旋桨叶片和发动机曲轴。这次检查的目的是确定六个连接螺栓失效的性质和可能的原因。在视觉和低倍镜检查中主要发现疲劳失效和磨损的迹象。断裂面显示,4个螺栓的螺纹和2个螺栓的杆部开始出现故障。四个螺栓的失效主要是由于拉伸载荷,而另外两个螺栓的失效主要是由于弯曲载荷。结果表明,故障是由于螺栓安装力矩不当造成的。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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