Failure Analysis of an Automobile Weldment

S. Edelglass
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Abstract

A front-wheel drive hatchback automobile was involved in a severe front end impact. Failure analysis of the automobile revealed only a single sound spot weld in each of two 66 cm (26 in.) sections of both upper and lower floor sill flanges. Consequently, upon impact, the floor pan separated from the rocker panel, buckled and rotated upward and forward. This introduced slack in the seat belts since their retractors, being anchored to the floor pan, also rotated forward. Although not contributory to the accident itself, the faulty welds were responsible in part for the severity of the injuries sustained by the driver. The faulty welds in the unit body were apparently a consequence of improper settings of parameters on a multihead electrical resistance spot welding machine. Lack of appreciation of the hazard associated with failure of this weldment may have contributed to the low frequency of their physical inspection during production. A similar case involving faulty welds in a fuel delivery truck is also discussed.
某汽车焊件失效分析
一辆前轮驱动的掀背式汽车发生了严重的前端碰撞。对汽车的故障分析显示,上下两个66厘米(26英寸)的底板法兰各有一个完好的点焊。因此,在撞击时,底板与摇臂板分离,弯曲并向上和向前旋转。这导致安全带松弛,因为安全带的牵引器被固定在底板上,也向前旋转。虽然不是造成事故本身的原因,但有缺陷的焊接是造成司机严重受伤的部分原因。机组本体焊缝故障显然是多头电阻点焊机参数设置不当造成的。由于缺乏对焊接件失效相关危害的认识,可能导致生产过程中对其进行物理检查的频率较低。还讨论了一个类似的案例,涉及燃料输送卡车的焊接缺陷。
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