Rectifying an Excessive Vibration Issue in Shallow Foundation with Permeation Grouting: A Case Study

J. Oetomo, Rizky Satria Putranto
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Abstract

Large vibrating machines are integral part of industrial facility. This paper describes the case example of excessive vibration, encountered in one of the machine foundations in such facility, as well as the corresponding rectification works. This vibrating machine was built on shallow foundation sitting on compacted sand fill layer; the foundation self-weight is more than eight (8) times of the equipment weight. The block foundation dimension is about 7.0 x 1.7 x 1.7 m3. The vibrating machine frequency (which sits above the foundation) is 450 rpm, with a relatively large impulsive cyclic load. In this paper, firstly, the potential root cause of this vibration issue is explored. Thereafter, considerations for the rectification works are described; in this case, a permeation grouting technique, using low-viscosity cement grout is chosen. The work method for this ground improvement works, including the completion criteria are described. Post-improvement vibration measurement indicates that the measured vibration is within the accepted vibration limit, indicating a successful improvement work.
渗透灌浆治理浅基础过振问题的实例研究
大型振动机是工业设备的重要组成部分。本文介绍了该设施某机器基础振动过大的实例,以及相应的整改工作。该振动机建在压实填砂层上的浅基础上;基础自重大于设备自重的8倍。砌块基础尺寸约为7.0 × 1.7 × 1.7 m3。振动机频率(位于基础上方)为450转/分,具有较大的脉冲循环载荷。本文首先探讨了产生该振动问题的潜在根本原因。随后,阐述了对修复工程的考虑;在这种情况下,采用低粘度水泥灌浆的渗透灌浆技术。介绍了该地基改善工程的施工方法及完成标准。改进后的振动测量表明,测量的振动在可接受的振动范围内,表明改进工作成功。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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