{"title":"Repair of Berth Faces at Port of Montreal with Fiber-Reinforced Shotcrete","authors":"D. Morgan, A. Lobo, L. Rich","doi":"10.14359/5713","DOIUrl":null,"url":null,"abstract":"This paper describes a prototype construction project in which about two thirds of a berth face, 122 m long and 7.1 m high, was repaired with a synthetic fiber reinforced shotcrete and the remaining third with a steel fiber reinforced shotcrete. The synthetic fiber used was a new mono-filament polyolefin fiber, 26 mm long x 0.38 mm diameter added at an addition rate of 1.25% by volume of shotcrete. The deformed steel fiber, 38 mm long, was added at an addition rate of 0.75% by volume of the shotcrete. The shotcrete used was air entrained, silica fume modified, supplied by transit mixers from a central mix plant and applied by the wet mix shotcrete process. The remedial design, shotcrete mixture designs, preconstruction mock up production and quality control testing are described as well, and a summary of construction quality control test results is provided.","PeriodicalId":148554,"journal":{"name":"SP-185: High-Performance Fiber Reinforced Concrete in Infrastructural Repair and Retrofit","volume":"1 1","pages":"0"},"PeriodicalIF":0.0000,"publicationDate":"2000-02-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"SP-185: High-Performance Fiber Reinforced Concrete in Infrastructural Repair and Retrofit","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.14359/5713","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0
Abstract
This paper describes a prototype construction project in which about two thirds of a berth face, 122 m long and 7.1 m high, was repaired with a synthetic fiber reinforced shotcrete and the remaining third with a steel fiber reinforced shotcrete. The synthetic fiber used was a new mono-filament polyolefin fiber, 26 mm long x 0.38 mm diameter added at an addition rate of 1.25% by volume of shotcrete. The deformed steel fiber, 38 mm long, was added at an addition rate of 0.75% by volume of the shotcrete. The shotcrete used was air entrained, silica fume modified, supplied by transit mixers from a central mix plant and applied by the wet mix shotcrete process. The remedial design, shotcrete mixture designs, preconstruction mock up production and quality control testing are described as well, and a summary of construction quality control test results is provided.